[ Upstream commit d897a4ab11 ]
Don't allow the TAI-UTC offset of the system clock to be set by adjtimex()
to a value larger than 100000 seconds.
This prevents an overflow in the conversion to int, prevents the CLOCK_TAI
clock from getting too far ahead of the CLOCK_REALTIME clock, and it is
still large enough to allow leap seconds to be inserted at the maximum rate
currently supported by the kernel (once per day) for the next ~270 years,
however unlikely it is that someone can survive a catastrophic event which
slowed down the rotation of the Earth so much.
Reported-by: Weikang shi <swkhack@gmail.com>
Signed-off-by: Miroslav Lichvar <mlichvar@redhat.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: John Stultz <john.stultz@linaro.org>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Richard Cochran <richardcochran@gmail.com>
Cc: Stephen Boyd <sboyd@kernel.org>
Link: https://lkml.kernel.org/r/20190618154713.20929-1-mlichvar@redhat.com
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit fdc6bae940 ]
The ADJ_TAI adjtimex mode sets the TAI-UTC offset of the system clock.
It is typically set by NTP/PTP implementations and it is automatically
updated by the kernel on leap seconds. The initial value is zero (which
applications may interpret as unknown), but this value cannot be set by
adjtimex. This limitation seems to go back to the original "nanokernel"
implementation by David Mills.
Change the ADJ_TAI check to accept zero as a valid TAI-UTC offset in
order to allow setting it back to the initial value.
Fixes: 153b5d054a ("ntp: support for TAI")
Suggested-by: Ondrej Mosnacek <omosnace@redhat.com>
Signed-off-by: Miroslav Lichvar <mlichvar@redhat.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: John Stultz <john.stultz@linaro.org>
Cc: Richard Cochran <richardcochran@gmail.com>
Cc: Prarit Bhargava <prarit@redhat.com>
Link: https://lkml.kernel.org/r/20190417084833.7401-1-mlichvar@redhat.com
Signed-off-by: Sasha Levin <sashal@kernel.org>
The timer_stats facility should filter and translate PIDs if opened
from a non-initial PID namespace, to avoid leaking information about
the wider system. It should also not show kernel virtual addresses.
Unfortunately it has now been removed upstream (as redundant)
instead of being fixed.
For stable, fix the leak by restricting access to root only. A
similar change was already made for the /proc/timer_list file.
Signed-off-by: Ben Hutchings <ben@decadent.org.uk>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 78c9c4dfbf ]
The posix timer overrun handling is broken because the forwarding functions
can return a huge number of overruns which does not fit in an int. As a
consequence timer_getoverrun(2) and siginfo::si_overrun can turn into
random number generators.
The k_clock::timer_forward() callbacks return a 64 bit value now. Make
k_itimer::ti_overrun[_last] 64bit as well, so the kernel internal
accounting is correct. 3Remove the temporary (int) casts.
Add a helper function which clamps the overrun value returned to user space
via timer_getoverrun(2) or siginfo::si_overrun limited to a positive value
between 0 and INT_MAX. INT_MAX is an indicator for user space that the
overrun value has been clamped.
Reported-by: Team OWL337 <icytxw@gmail.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Acked-by: John Stultz <john.stultz@linaro.org>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: Michael Kerrisk <mtk.manpages@gmail.com>
Link: https://lkml.kernel.org/r/20180626132705.018623573@linutronix.de
[florian: Make patch apply to v4.9.135]
Signed-off-by: Florian Fainelli <f.fainelli@gmail.com>
Reviewed-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 5f936e19cc ]
Air Icy reported:
UBSAN: Undefined behaviour in kernel/time/alarmtimer.c:811:7
signed integer overflow:
1529859276030040771 + 9223372036854775807 cannot be represented in type 'long long int'
Call Trace:
alarm_timer_nsleep+0x44c/0x510 kernel/time/alarmtimer.c:811
__do_sys_clock_nanosleep kernel/time/posix-timers.c:1235 [inline]
__se_sys_clock_nanosleep kernel/time/posix-timers.c:1213 [inline]
__x64_sys_clock_nanosleep+0x326/0x4e0 kernel/time/posix-timers.c:1213
do_syscall_64+0xb8/0x3a0 arch/x86/entry/common.c:290
alarm_timer_nsleep() uses ktime_add() to add the current time and the
relative expiry value. ktime_add() has no sanity checks so the addition
can overflow when the relative timeout is large enough.
Use ktime_add_safe() which has the necessary sanity checks in place and
limits the result to the valid range.
Fixes: 9a7adcf5c6 ("timers: Posix interface for alarm-timers")
Reported-by: Team OWL337 <icytxw@gmail.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: John Stultz <john.stultz@linaro.org>
Link: https://lkml.kernel.org/r/alpine.DEB.2.21.1807020926360.1595@nanos.tec.linutronix.de
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 363e934d88 ]
timer_base::must_forward_clock is indicating that the base clock might be
stale due to a long idle sleep.
The forwarding of the base clock takes place in the timer softirq or when a
timer is enqueued to a base which is idle. If the enqueue of timer to an
idle base happens from a remote CPU, then the following race can happen:
CPU0 CPU1
run_timer_softirq mod_timer
base = lock_timer_base(timer);
base->must_forward_clk = false
if (base->must_forward_clk)
forward(base); -> skipped
enqueue_timer(base, timer, idx);
-> idx is calculated high due to
stale base
unlock_timer_base(timer);
base = lock_timer_base(timer);
forward(base);
The root cause is that timer_base::must_forward_clk is cleared outside the
timer_base::lock held region, so the remote queuing CPU observes it as
cleared, but the base clock is still stale. This can cause large
granularity values for timers, i.e. the accuracy of the expiry time
suffers.
Prevent this by clearing the flag with timer_base::lock held, so that the
forwarding takes place before the cleared flag is observable by a remote
CPU.
Signed-off-by: Gaurav Kohli <gkohli@codeaurora.org>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: john.stultz@linaro.org
Cc: sboyd@kernel.org
Cc: linux-arm-msm@vger.kernel.org
Link: https://lkml.kernel.org/r/1533199863-22748-1-git-send-email-gkohli@codeaurora.org
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit abcbcb80cd upstream.
For the common cases where 1000 is a multiple of HZ, or HZ is a multiple of
1000, jiffies_to_msecs() never returns zero when passed a non-zero time
period.
However, if HZ > 1000 and not an integer multiple of 1000 (e.g. 1024 or
1200, as used on alpha and DECstation), jiffies_to_msecs() may return zero
for small non-zero time periods. This may break code that relies on
receiving back a non-zero value.
jiffies_to_usecs() does not need such a fix: one jiffy can only be less
than one µs if HZ > 1000000, and such large values of HZ are already
rejected at build time, twice:
- include/linux/jiffies.h does #error if HZ >= 12288,
- kernel/time/time.c has BUILD_BUG_ON(HZ > USEC_PER_SEC).
Broken since forever.
Signed-off-by: Geert Uytterhoeven <geert@linux-m68k.org>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Reviewed-by: Arnd Bergmann <arnd@arndb.de>
Cc: John Stultz <john.stultz@linaro.org>
Cc: Stephen Boyd <sboyd@kernel.org>
Cc: linux-alpha@vger.kernel.org
Cc: linux-mips@linux-mips.org
Cc: stable@vger.kernel.org
Link: https://lkml.kernel.org/r/20180622143357.7495-1-geert@linux-m68k.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 0107042768 ]
On systems with a large number of CPUs, running sysrq-<q> can cause
watchdog timeouts. There are two slow sections of code in the sysrq-<q>
path in timer_list.c.
1. print_active_timers() - This function is called by print_cpu() and
contains a slow goto loop. On a machine with hundreds of CPUs, this
loop took approximately 100ms for the first CPU in a NUMA node.
(Subsequent CPUs in the same node ran much quicker.) The total time
to print all of the CPUs is ultimately long enough to trigger the
soft lockup watchdog.
2. print_tickdevice() - This function outputs a large amount of textual
information. This function also took approximately 100ms per CPU.
Since sysrq-<q> is not a performance critical path, there should be no
harm in touching the nmi watchdog in both slow sections above. Touching
it in just one location was insufficient on systems with hundreds of
CPUs as occasional timeouts were still observed during testing.
This issue was observed on an Oracle T7 machine with 128 CPUs, but I
anticipate it may affect other systems with similarly large numbers of
CPUs.
Signed-off-by: Tom Hromatka <tom.hromatka@oracle.com>
Reviewed-by: Rob Gardner <rob.gardner@oracle.com>
Signed-off-by: John Stultz <john.stultz@linaro.org>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 1b8955bc5a ]
The scheduler clock framework may not use the correct timeout for the clock
wrap. This happens when a new clock driver calls sched_clock_register()
after the kernel called sched_clock_postinit(). In this case the clock wrap
timeout is too long thus sched_clock_poll() is called too late and the clock
already wrapped.
On my ARM system the scheduler was no longer scheduling any other task than
the idle task because the sched_clock() wrapped.
Signed-off-by: David Engraf <david.engraf@sysgo.com>
Signed-off-by: John Stultz <john.stultz@linaro.org>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit c52232a49e upstream.
On CPU hotunplug the enqueued timers of the unplugged CPU are migrated to a
live CPU. This happens from the control thread which initiated the unplug.
If the CPU on which the control thread runs came out from a longer idle
period then the base clock of that CPU might be stale because the control
thread runs prior to any event which forwards the clock.
In such a case the timers from the unplugged CPU are queued on the live CPU
based on the stale clock which can cause large delays due to increased
granularity of the outer timer wheels which are far away from base:;clock.
But there is a worse problem than that. The following sequence of events
illustrates it:
- CPU0 timer1 is queued expires = 59969 and base->clk = 59131.
The timer is queued at wheel level 2, with resulting expiry time = 60032
(due to level granularity).
- CPU1 enters idle @60007, with next timer expiry @60020.
- CPU0 is hotplugged at @60009
- CPU1 exits idle and runs the control thread which migrates the
timers from CPU0
timer1 is now queued in level 0 for immediate handling in the next
softirq because the requested expiry time 59969 is before CPU1 base->clk
60007
- CPU1 runs code which forwards the base clock which succeeds because the
next expiring timer. which was collected at idle entry time is still set
to 60020.
So it forwards beyond 60007 and therefore misses to expire the migrated
timer1. That timer gets expired when the wheel wraps around again, which
takes between 63 and 630ms depending on the HZ setting.
Address both problems by invoking forward_timer_base() for the control CPUs
timer base. All other places, which might run into a similar problem
(mod_timer()/add_timer_on()) already invoke forward_timer_base() to avoid
that.
[ tglx: Massaged comment and changelog ]
Fixes: a683f390b9 ("timers: Forward the wheel clock whenever possible")
Co-developed-by: Neeraj Upadhyay <neeraju@codeaurora.org>
Signed-off-by: Neeraj Upadhyay <neeraju@codeaurora.org>
Signed-off-by: Lingutla Chandrasekhar <clingutla@codeaurora.org>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Anna-Maria Gleixner <anna-maria@linutronix.de>
Cc: linux-arm-msm@vger.kernel.org
Cc: stable@vger.kernel.org
Link: https://lkml.kernel.org/r/20180118115022.6368-1-clingutla@codeaurora.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit cef31d9af9 upstream.
timer_create() specifies via sigevent->sigev_notify the signal delivery for
the new timer. The valid modes are SIGEV_NONE, SIGEV_SIGNAL, SIGEV_THREAD
and (SIGEV_SIGNAL | SIGEV_THREAD_ID).
The sanity check in good_sigevent() is only checking the valid combination
for the SIGEV_THREAD_ID bit, i.e. SIGEV_SIGNAL, but if SIGEV_THREAD_ID is
not set it accepts any random value.
This has no real effects on the posix timer and signal delivery code, but
it affects show_timer() which handles the output of /proc/$PID/timers. That
function uses a string array to pretty print sigev_notify. The access to
that array has no bound checks, so random sigev_notify cause access beyond
the array bounds.
Add proper checks for the valid notify modes and remove the SIGEV_THREAD_ID
masking from various code pathes as SIGEV_NONE can never be set in
combination with SIGEV_THREAD_ID.
Reported-by: Eric Biggers <ebiggers3@gmail.com>
Reported-by: Dmitry Vyukov <dvyukov@google.com>
Reported-by: Alexey Dobriyan <adobriyan@gmail.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: John Stultz <john.stultz@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit d5421ea43d upstream.
The hrtimer interrupt code contains a hang detection and mitigation
mechanism, which prevents that a long delayed hrtimer interrupt causes a
continous retriggering of interrupts which prevent the system from making
progress. If a hang is detected then the timer hardware is programmed with
a certain delay into the future and a flag is set in the hrtimer cpu base
which prevents newly enqueued timers from reprogramming the timer hardware
prior to the chosen delay. The subsequent hrtimer interrupt after the delay
clears the flag and resumes normal operation.
If such a hang happens in the last hrtimer interrupt before a CPU is
unplugged then the hang_detected flag is set and stays that way when the
CPU is plugged in again. At that point the timer hardware is not armed and
it cannot be armed because the hang_detected flag is still active, so
nothing clears that flag. As a consequence the CPU does not receive hrtimer
interrupts and no timers expire on that CPU which results in RCU stalls and
other malfunctions.
Clear the flag along with some other less critical members of the hrtimer
cpu base to ensure starting from a clean state when a CPU is plugged in.
Thanks to Paul, Sebastian and Anna-Maria for their help to get down to the
root cause of that hard to reproduce heisenbug. Once understood it's
trivial and certainly justifies a brown paperbag.
Fixes: 41d2e49493 ("hrtimer: Tune hrtimer_interrupt hang logic")
Reported-by: Paul E. McKenney <paulmck@linux.vnet.ibm.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: Sebastian Sewior <bigeasy@linutronix.de>
Cc: Anna-Maria Gleixner <anna-maria@linutronix.de>
Link: https://lkml.kernel.org/r/alpine.DEB.2.20.1801261447590.2067@nanos
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 5d62c183f9 upstream.
The conditions in irq_exit() to invoke tick_nohz_irq_exit() which
subsequently invokes tick_nohz_stop_sched_tick() are:
if ((idle_cpu(cpu) && !need_resched()) || tick_nohz_full_cpu(cpu))
If need_resched() is not set, but a timer softirq is pending then this is
an indication that the softirq code punted and delegated the execution to
softirqd. need_resched() is not true because the current interrupted task
takes precedence over softirqd.
Invoking tick_nohz_irq_exit() in this case can cause an endless loop of
timer interrupts because the timer wheel contains an expired timer, but
softirqs are not yet executed. So it returns an immediate expiry request,
which causes the timer to fire immediately again. Lather, rinse and
repeat....
Prevent that by adding a check for a pending timer soft interrupt to the
conditions in tick_nohz_stop_sched_tick() which avoid calling
get_next_timer_interrupt(). That keeps the tick sched timer on the tick and
prevents a repetitive programming of an already expired timer.
Reported-by: Sebastian Siewior <bigeasy@linutronix.d>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Acked-by: Frederic Weisbecker <fweisbec@gmail.com>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: Paul McKenney <paulmck@linux.vnet.ibm.com>
Cc: Anna-Maria Gleixner <anna-maria@linutronix.de>
Cc: Sebastian Siewior <bigeasy@linutronix.de>
Link: https://lkml.kernel.org/r/alpine.DEB.2.20.1712272156050.2431@nanos
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit ced6d5c11d upstream.
During boot and before base::nohz_active is set in the timer bases, deferrable
timers are enqueued into the standard timer base. This works correctly as
long as base::nohz_active is false.
Once it base::nohz_active is set and a timer which was enqueued before that
is accessed the lock selector code choses the lock of the deferred
base. This causes unlocked access to the standard base and in case the
timer is removed it does not clear the pending flag in the standard base
bitmap which causes get_next_timer_interrupt() to return bogus values.
To prevent that, the deferrable timers must be enqueued in the deferrable
base, even when base::nohz_active is not set. Those deferrable timers also
need to be expired unconditional.
Fixes: 500462a9de ("timers: Switch to a non-cascading wheel")
Signed-off-by: Anna-Maria Gleixner <anna-maria@linutronix.de>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Reviewed-by: Frederic Weisbecker <fweisbec@gmail.com>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: Sebastian Siewior <bigeasy@linutronix.de>
Cc: rt@linutronix.de
Cc: Paul McKenney <paulmck@linux.vnet.ibm.com>
Link: https://lkml.kernel.org/r/20171222145337.633328378@linutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 336a9cde10 ]
commit 82e88ff1ea ("hrtimer: Revert CLOCK_MONOTONIC_RAW support") removed
unfortunately a sanity check in the hrtimer code which was part of that
MONOTONIC_RAW patch series.
It would have caught the bogus usage of CLOCK_MONOTONIC_RAW in the wireless
code. So bring it back.
It is way too easy to take any random clockid and feed it to the hrtimer
subsystem. At best, it gets mapped to a monotonic base, but it would be
better to just catch illegal values as early as possible.
Detect invalid clockids, map them to CLOCK_MONOTONIC and emit a warning.
[ tglx: Replaced the BUG by a WARN and gracefully map to CLOCK_MONOTONIC ]
Signed-off-by: Marc Zyngier <marc.zyngier@arm.com>
Cc: Tomasz Nowicki <tn@semihalf.com>
Cc: Christoffer Dall <christoffer.dall@linaro.org>
Link: http://lkml.kernel.org/r/1452879670-16133-3-git-send-email-marc.zyngier@arm.com
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Sasha Levin <alexander.levin@verizon.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 2fe59f507a upstream.
When a timer base is idle, it is forwarded when a new timer is added
to ensure that granularity does not become excessive. When not idle,
the timer tick is expected to increment the base.
However there are several problems:
- If an existing timer is modified, the base is forwarded only after
the index is calculated.
- The base is not forwarded by add_timer_on.
- There is a window after a timer is restarted from a nohz idle, after
it is marked not-idle and before the timer tick on this CPU, where a
timer may be added but the ancient base does not get forwarded.
These result in excessive granularity (a 1 jiffy timeout can blow out
to 100s of jiffies), which cause the rcu lockup detector to trigger,
among other things.
Fix this by keeping track of whether the timer base has been idle
since it was last run or forwarded, and if so then forward it before
adding a new timer.
There is still a case where mod_timer optimises the case of a pending
timer mod with the same expiry time, where the timer can see excessive
granularity relative to the new, shorter interval. A comment is added,
but it's not changed because it is an important fastpath for
networking.
This has been tested and found to fix the RCU softlockup messages.
Testing was also done with tracing to measure requested versus
achieved wakeup latencies for all non-deferrable timers in an idle
system (with no lockup watchdogs running). Wakeup latency relative to
absolute latency is calculated (note this suffers from round-up skew
at low absolute times) and analysed:
max avg std
upstream 506.0 1.20 4.68
patched 2.0 1.08 0.15
The bug was noticed due to the lockup detector Kconfig changes
dropping it out of people's .configs and resulting in larger base
clk skew When the lockup detectors are enabled, no CPU can go idle for
longer than 4 seconds, which limits the granularity errors.
Sub-optimal timer behaviour is observable on a smaller scale in that
case:
max avg std
upstream 9.0 1.05 0.19
patched 2.0 1.04 0.11
Fixes: Fixes: a683f390b9 ("timers: Forward the wheel clock whenever possible")
Signed-off-by: Nicholas Piggin <npiggin@gmail.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Jonathan Cameron <Jonathan.Cameron@huawei.com>
Tested-by: David Miller <davem@davemloft.net>
Cc: dzickus@redhat.com
Cc: sfr@canb.auug.org.au
Cc: mpe@ellerman.id.au
Cc: Stephen Boyd <sboyd@codeaurora.org>
Cc: linuxarm@huawei.com
Cc: abdhalee@linux.vnet.ibm.com
Cc: John Stultz <john.stultz@linaro.org>
Cc: akpm@linux-foundation.org
Cc: paulmck@linux.vnet.ibm.com
Cc: torvalds@linux-foundation.org
Link: http://lkml.kernel.org/r/20170822084348.21436-1-npiggin@gmail.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 3d88d56c58 upstream.
Due to how the MONOTONIC_RAW accumulation logic was handled,
there is the potential for a 1ns discontinuity when we do
accumulations. This small discontinuity has for the most part
gone un-noticed, but since ARM64 enabled CLOCK_MONOTONIC_RAW
in their vDSO clock_gettime implementation, we've seen failures
with the inconsistency-check test in kselftest.
This patch addresses the issue by using the same sub-ns
accumulation handling that CLOCK_MONOTONIC uses, which avoids
the issue for in-kernel users.
Since the ARM64 vDSO implementation has its own clock_gettime
calculation logic, this patch reduces the frequency of errors,
but failures are still seen. The ARM64 vDSO will need to be
updated to include the sub-nanosecond xtime_nsec values in its
calculation for this issue to be completely fixed.
Signed-off-by: John Stultz <john.stultz@linaro.org>
Tested-by: Daniel Mentz <danielmentz@google.com>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Kevin Brodsky <kevin.brodsky@arm.com>
Cc: Richard Cochran <richardcochran@gmail.com>
Cc: Stephen Boyd <stephen.boyd@linaro.org>
Cc: Will Deacon <will.deacon@arm.com>
Cc: Miroslav Lichvar <mlichvar@redhat.com>
Link: http://lkml.kernel.org/r/1496965462-20003-3-git-send-email-john.stultz@linaro.org
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit ceea5e3771 upstream.
In tests, which excercise switching of clocksources, a NULL
pointer dereference can be observed on AMR64 platforms in the
clocksource read() function:
u64 clocksource_mmio_readl_down(struct clocksource *c)
{
return ~(u64)readl_relaxed(to_mmio_clksrc(c)->reg) & c->mask;
}
This is called from the core timekeeping code via:
cycle_now = tkr->read(tkr->clock);
tkr->read is the cached tkr->clock->read() function pointer.
When the clocksource is changed then tkr->clock and tkr->read
are updated sequentially. The code above results in a sequential
load operation of tkr->read and tkr->clock as well.
If the store to tkr->clock hits between the loads of tkr->read
and tkr->clock, then the old read() function is called with the
new clock pointer. As a consequence the read() function
dereferences a different data structure and the resulting 'reg'
pointer can point anywhere including NULL.
This problem was introduced when the timekeeping code was
switched over to use struct tk_read_base. Before that, it was
theoretically possible as well when the compiler decided to
reload clock in the code sequence:
now = tk->clock->read(tk->clock);
Add a helper function which avoids the issue by reading
tk_read_base->clock once into a local variable clk and then issue
the read function via clk->read(clk). This guarantees that the
read() function always gets the proper clocksource pointer handed
in.
Since there is now no use for the tkr.read pointer, this patch
also removes it, and to address stopping the fast timekeeper
during suspend/resume, it introduces a dummy clocksource to use
rather then just a dummy read function.
Signed-off-by: John Stultz <john.stultz@linaro.org>
Acked-by: Ingo Molnar <mingo@kernel.org>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Richard Cochran <richardcochran@gmail.com>
Cc: Stephen Boyd <stephen.boyd@linaro.org>
Cc: Miroslav Lichvar <mlichvar@redhat.com>
Cc: Daniel Mentz <danielmentz@google.com>
Link: http://lkml.kernel.org/r/1496965462-20003-2-git-send-email-john.stultz@linaro.org
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit ff86bf0c65 upstream.
The alarmtimer code has another source of potentially rearming itself too
fast. Interval timers with a very samll interval have a similar CPU hog
effect as the previously fixed overflow issue.
The reason is that alarmtimers do not implement the normal protection
against this kind of problem which the other posix timer use:
timer expires -> queue signal -> deliver signal -> rearm timer
This scheme brings the rearming under scheduler control and prevents
permanently firing timers which hog the CPU.
Bringing this scheme to the alarm timer code is a major overhaul because it
lacks all the necessary mechanisms completely.
So for a quick fix limit the interval to one jiffie. This is not
problematic in practice as alarmtimers are usually backed by an RTC for
suspend which have 1 second resolution. It could be therefor argued that
the resolution of this clock should be set to 1 second in general, but
that's outside the scope of this fix.
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: Kostya Serebryany <kcc@google.com>
Cc: syzkaller <syzkaller@googlegroups.com>
Cc: John Stultz <john.stultz@linaro.org>
Cc: Dmitry Vyukov <dvyukov@google.com>
Link: http://lkml.kernel.org/r/20170530211655.896767100@linutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit f4781e76f9 upstream.
Andrey reported a alartimer related RCU stall while fuzzing the kernel with
syzkaller.
The reason for this is an overflow in ktime_add() which brings the
resulting time into negative space and causes immediate expiry of the
timer. The following rearm with a small interval does not bring the timer
back into positive space due to the same issue.
This results in a permanent firing alarmtimer which hogs the CPU.
Use ktime_add_safe() instead which detects the overflow and clamps the
result to KTIME_SEC_MAX.
Reported-by: Andrey Konovalov <andreyknvl@google.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: Kostya Serebryany <kcc@google.com>
Cc: syzkaller <syzkaller@googlegroups.com>
Cc: John Stultz <john.stultz@linaro.org>
Cc: Dmitry Vyukov <dvyukov@google.com>
Link: http://lkml.kernel.org/r/20170530211655.802921648@linutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 9c1645727b upstream.
The clocksource delta to nanoseconds conversion is using signed math, but
the delta is unsigned. This makes the conversion space smaller than
necessary and in case of a multiplication overflow the conversion can
become negative. The conversion is done with scaled math:
s64 nsec_delta = ((s64)clkdelta * clk->mult) >> clk->shift;
Shifting a signed integer right obvioulsy preserves the sign, which has
interesting consequences:
- Time jumps backwards
- __iter_div_u64_rem() which is used in one of the calling code pathes
will take forever to piecewise calculate the seconds/nanoseconds part.
This has been reported by several people with different scenarios:
David observed that when stopping a VM with a debugger:
"It was essentially the stopped by debugger case. I forget exactly why,
but the guest was being explicitly stopped from outside, it wasn't just
scheduling lag. I think it was something in the vicinity of 10 minutes
stopped."
When lifting the stop the machine went dead.
The stopped by debugger case is not really interesting, but nevertheless it
would be a good thing not to die completely.
But this was also observed on a live system by Liav:
"When the OS is too overloaded, delta will get a high enough value for the
msb of the sum delta * tkr->mult + tkr->xtime_nsec to be set, and so
after the shift the nsec variable will gain a value similar to
0xffffffffff000000."
Unfortunately this has been reintroduced recently with commit 6bd58f09e1
("time: Add cycles to nanoseconds translation"). It had been fixed a year
ago already in commit 35a4933a89 ("time: Avoid signed overflow in
timekeeping_get_ns()").
Though it's not surprising that the issue has been reintroduced because the
function itself and the whole call chain uses s64 for the result and the
propagation of it. The change in this recent commit is subtle:
s64 nsec;
- nsec = (d * m + n) >> s:
+ nsec = d * m + n;
+ nsec >>= s;
d being type of cycle_t adds another level of obfuscation.
This wouldn't have happened if the previous change to unsigned computation
would have made the 'nsec' variable u64 right away and a follow up patch
had cleaned up the whole call chain.
There have been patches submitted which basically did a revert of the above
patch leaving everything else unchanged as signed. Back to square one. This
spawned a admittedly pointless discussion about potential users which rely
on the unsigned behaviour until someone pointed out that it had been fixed
before. The changelogs of said patches added further confusion as they made
finally false claims about the consequences for eventual users which expect
signed results.
Despite delta being cycle_t, aka. u64, it's very well possible to hand in
a signed negative value and the signed computation will happily return the
correct result. But nobody actually sat down and analyzed the code which
was added as user after the propably unintended signed conversion.
Though in sensitive code like this it's better to analyze it proper and
make sure that nothing relies on this than hunting the subtle wreckage half
a year later. After analyzing all call chains it stands that no caller can
hand in a negative value (which actually would work due to the s64 cast)
and rely on the signed math to do the right thing.
Change the conversion function to unsigned math. The conversion of all call
chains is done in a follow up patch.
This solves the starvation issue, which was caused by the negative result,
but it does not solve the underlying problem. It merily procrastinates
it. When the timekeeper update is deferred long enough that the unsigned
multiplication overflows, then time going backwards is observable again.
It does neither solve the issue of clocksources with a small counter width
which will wrap around possibly several times and cause random time stamps
to be generated. But those are usually not found on systems used for
virtualization, so this is likely a non issue.
I took the liberty to claim authorship for this simply because
analyzing all callsites and writing the changelog took substantially
more time than just making the simple s/s64/u64/ change and ignore the
rest.
Fixes: 6bd58f09e1 ("time: Add cycles to nanoseconds translation")
Reported-by: David Gibson <david@gibson.dropbear.id.au>
Reported-by: Liav Rehana <liavr@mellanox.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Reviewed-by: David Gibson <david@gibson.dropbear.id.au>
Acked-by: Peter Zijlstra (Intel) <peterz@infradead.org>
Cc: Parit Bhargava <prarit@redhat.com>
Cc: Laurent Vivier <lvivier@redhat.com>
Cc: "Christopher S. Hall" <christopher.s.hall@intel.com>
Cc: Chris Metcalf <cmetcalf@mellanox.com>
Cc: Richard Cochran <richardcochran@gmail.com>
Cc: John Stultz <john.stultz@linaro.org>
Link: http://lkml.kernel.org/r/20161208204228.688545601@linutronix.de
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When a timer is enqueued we try to forward the timer base clock. This
mechanism has two issues:
1) Forwarding a remote base unlocked
The forwarding function is called from get_target_base() with the current
timer base lock held. But if the new target base is a different base than
the current base (can happen with NOHZ, sigh!) then the forwarding is done
on an unlocked base. This can lead to corruption of base->clk.
Solution is simple: Invoke the forwarding after the target base is locked.
2) Possible corruption due to jiffies advancing
This is similar to the issue in get_net_timer_interrupt() which was fixed
in the previous patch. jiffies can advance between check and assignement
and therefore advancing base->clk beyond the next expiry value.
So we need to read jiffies into a local variable once and do the checks and
assignment with the local copy.
Fixes: a683f390b93f("timers: Forward the wheel clock whenever possible")
Reported-by: Ashton Holmes <scoopta@gmail.com>
Reported-by: Michael Thayer <michael.thayer@oracle.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Michal Necasek <michal.necasek@oracle.com>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: knut.osmundsen@oracle.com
Cc: stable@vger.kernel.org
Cc: stern@rowland.harvard.edu
Cc: rt@linutronix.de
Link: http://lkml.kernel.org/r/20161022110552.253640125@linutronix.de
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Ashton and Michael reported, that kernel versions 4.8 and later suffer from
USB timeouts which are caused by the timer wheel rework.
This is caused by a bug in the base clock forwarding mechanism, which leads
to timers expiring early. The scenario which leads to this is:
run_timers()
while (jiffies >= base->clk) {
collect_expired_timers();
base->clk++;
expire_timers();
}
So base->clk = jiffies + 1. Now the cpu goes idle:
idle()
get_next_timer_interrupt()
nextevt = __next_time_interrupt();
if (time_after(nextevt, base->clk))
base->clk = jiffies;
jiffies has not advanced since run_timers(), so this assignment effectively
decrements base->clk by one.
base->clk is the index into the timer wheel arrays. So let's assume the
following state after the base->clk increment in run_timers():
jiffies = 0
base->clk = 1
A timer gets enqueued with an expiry delta of 63 ticks (which is the case
with the USB timeout and HZ=250) so the resulting bucket index is:
base->clk + delta = 1 + 63 = 64
The timer goes into the first wheel level. The array size is 64 so it ends
up in bucket 0, which is correct as it takes 63 ticks to advance base->clk
to index into bucket 0 again.
If the cpu goes idle before jiffies advance, then the bug in the forwarding
mechanism sets base->clk back to 0, so the next invocation of run_timers()
at the next tick will index into bucket 0 and therefore expire the timer 62
ticks too early.
Instead of blindly setting base->clk to jiffies we must make the forwarding
conditional on jiffies > base->clk, but we cannot use jiffies for this as
we might run into the following issue:
if (time_after(jiffies, base->clk) {
if (time_after(nextevt, base->clk))
base->clk = jiffies;
jiffies can increment between the check and the assigment far enough to
advance beyond nextevt. So we need to use a stable value for checking.
get_next_timer_interrupt() has the basej argument which is the jiffies
value snapshot taken in the calling code. So we can just that.
Thanks to Ashton for bisecting and providing trace data!
Fixes: a683f390b9 ("timers: Forward the wheel clock whenever possible")
Reported-by: Ashton Holmes <scoopta@gmail.com>
Reported-by: Michael Thayer <michael.thayer@oracle.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Michal Necasek <michal.necasek@oracle.com>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: knut.osmundsen@oracle.com
Cc: stable@vger.kernel.org
Cc: stern@rowland.harvard.edu
Cc: rt@linutronix.de
Link: http://lkml.kernel.org/r/20161022110552.175308322@linutronix.de
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Linus stumbled over the unlocked modification of the timer expiry value in
mod_timer() which is an optimization for timers which stay in the same
bucket - due to the bucket granularity - despite their expiry time getting
updated.
The optimization itself still makes sense even if we take the lock, because
in case that the bucket stays the same, we avoid the pointless
queue/enqueue dance.
Make the check and the modification of timer->expires protected by the base
lock and shuffle the remaining code around so we can keep the lock held
when we actually have to requeue the timer to a different bucket.
Fixes: f00c0afdfa ("timers: Implement optimization for same expiry time in mod_timer()")
Reported-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Link: http://lkml.kernel.org/r/alpine.DEB.2.20.1610241711220.4983@nanos
Cc: stable@vger.kernel.org
Cc: Andrew Morton <akpm@linux-foundation.org>
Cc: Peter Zijlstra <peterz@infradead.org>
Pull gcc plugins update from Kees Cook:
"This adds a new gcc plugin named "latent_entropy". It is designed to
extract as much possible uncertainty from a running system at boot
time as possible, hoping to capitalize on any possible variation in
CPU operation (due to runtime data differences, hardware differences,
SMP ordering, thermal timing variation, cache behavior, etc).
At the very least, this plugin is a much more comprehensive example
for how to manipulate kernel code using the gcc plugin internals"
* tag 'gcc-plugins-v4.9-rc1' of git://git.kernel.org/pub/scm/linux/kernel/git/kees/linux:
latent_entropy: Mark functions with __latent_entropy
gcc-plugins: Add latent_entropy plugin
The __latent_entropy gcc attribute can be used only on functions and
variables. If it is on a function then the plugin will instrument it for
gathering control-flow entropy. If the attribute is on a variable then
the plugin will initialize it with random contents. The variable must
be an integer, an integer array type or a structure with integer fields.
These specific functions have been selected because they are init
functions (to help gather boot-time entropy), are called at unpredictable
times, or they have variable loops, each of which provide some level of
latent entropy.
Signed-off-by: Emese Revfy <re.emese@gmail.com>
[kees: expanded commit message]
Signed-off-by: Kees Cook <keescook@chromium.org>
can_stop_full_tick() has no check for offline cpus. So it allows to stop
the tick on an offline cpu from the interrupt return path, which is wrong
and subsequently makes irq_work_needs_cpu() warn about being called for an
offline cpu.
Commit f7ea0fd639 ("tick: Don't invoke tick_nohz_stop_sched_tick() if
the cpu is offline") added prevention for can_stop_idle_tick(), but forgot
to do the same in can_stop_full_tick(). Add it.
[ tglx: Massaged changelog ]
Signed-off-by: Wanpeng Li <wanpeng.li@hotmail.com>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: Frederic Weisbecker <fweisbec@gmail.com>
Link: http://lkml.kernel.org/r/1473245473-4463-1-git-send-email-wanpeng.li@hotmail.com
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
tick_nohz_start_idle() is prevented to be called if the idle tick can't
be stopped since commit 1f3b0f8243 ("tick/nohz: Optimize nohz idle
enter"). As a result, after suspend/resume the host machine, full dynticks
kvm guest will softlockup:
NMI watchdog: BUG: soft lockup - CPU#0 stuck for 26s! [swapper/0:0]
Call Trace:
default_idle+0x31/0x1a0
arch_cpu_idle+0xf/0x20
default_idle_call+0x2a/0x50
cpu_startup_entry+0x39b/0x4d0
rest_init+0x138/0x140
? rest_init+0x5/0x140
start_kernel+0x4c1/0x4ce
? set_init_arg+0x55/0x55
? early_idt_handler_array+0x120/0x120
x86_64_start_reservations+0x24/0x26
x86_64_start_kernel+0x142/0x14f
In addition, cat /proc/stat | grep cpu in guest or host:
cpu 398 16 5049 15754 5490 0 1 46 0 0
cpu0 206 5 450 0 0 0 1 14 0 0
cpu1 81 0 3937 3149 1514 0 0 9 0 0
cpu2 45 6 332 6052 2243 0 0 11 0 0
cpu3 65 2 328 6552 1732 0 0 11 0 0
The idle and iowait states are weird 0 for cpu0(housekeeping).
The bug is present in both guest and host kernels, and they both have
cpu0's idle and iowait states issue, however, host kernel's suspend/resume
path etc will touch watchdog to avoid the softlockup.
- The watchdog will not be touched in tick_nohz_stop_idle path (need be
touched since the scheduler stall is expected) if idle_active flags are
not detected.
- The idle and iowait states will not be accounted when exit idle loop
(resched or interrupt) if idle start time and idle_active flags are
not set.
This patch fixes it by reverting commit 1f3b0f8243 since can't stop
idle tick doesn't mean can't be idle.
Fixes: 1f3b0f8243 ("tick/nohz: Optimize nohz idle enter")
Signed-off-by: Wanpeng Li <wanpeng.li@hotmail.com>
Cc: Sanjeev Yadav<sanjeev.yadav@spreadtrum.com>
Cc: Gaurav Jindal<gaurav.jindal@spreadtrum.com>
Cc: stable@vger.kernel.org
Cc: kvm@vger.kernel.org
Cc: Radim Krčmář <rkrcmar@redhat.com>
Cc: Peter Zijlstra <peterz@infradead.org>
Cc: Paolo Bonzini <pbonzini@redhat.com>
Link: http://lkml.kernel.org/r/1472798303-4154-1-git-send-email-wanpeng.li@hotmail.com
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
I ran into this:
================================================================================
UBSAN: Undefined behaviour in kernel/time/time.c:783:2
signed integer overflow:
5273 + 9223372036854771711 cannot be represented in type 'long int'
CPU: 0 PID: 17363 Comm: trinity-c0 Not tainted 4.8.0-rc1+ #88
Hardware name: QEMU Standard PC (i440FX + PIIX, 1996), BIOS rel-1.9.3-0-ge2fc41e-prebuilt.qemu-project.org
04/01/2014
0000000000000000 ffff88011457f8f0 ffffffff82344f50 0000000041b58ab3
ffffffff84f98080 ffffffff82344ea4 ffff88011457f918 ffff88011457f8c8
ffff88011457f8e0 7fffffffffffefff ffff88011457f6d8 dffffc0000000000
Call Trace:
[<ffffffff82344f50>] dump_stack+0xac/0xfc
[<ffffffff82344ea4>] ? _atomic_dec_and_lock+0xc4/0xc4
[<ffffffff8242f4c8>] ubsan_epilogue+0xd/0x8a
[<ffffffff8242fc04>] handle_overflow+0x202/0x23d
[<ffffffff8242fa02>] ? val_to_string.constprop.6+0x11e/0x11e
[<ffffffff823c7837>] ? debug_smp_processor_id+0x17/0x20
[<ffffffff8131b581>] ? __sigqueue_free.part.13+0x51/0x70
[<ffffffff8146d4e0>] ? rcu_is_watching+0x110/0x110
[<ffffffff8242fc4d>] __ubsan_handle_add_overflow+0xe/0x10
[<ffffffff81476ef8>] timespec64_add_safe+0x298/0x340
[<ffffffff81476c60>] ? timespec_add_safe+0x330/0x330
[<ffffffff812f7990>] ? wait_noreap_copyout+0x1d0/0x1d0
[<ffffffff8184bf18>] poll_select_set_timeout+0xf8/0x170
[<ffffffff8184be20>] ? poll_schedule_timeout+0x2b0/0x2b0
[<ffffffff813aa9bb>] ? __might_sleep+0x5b/0x260
[<ffffffff833c8a87>] __sys_recvmmsg+0x107/0x790
[<ffffffff833c8980>] ? SyS_recvmsg+0x20/0x20
[<ffffffff81486378>] ? hrtimer_start_range_ns+0x3b8/0x1380
[<ffffffff845f8bfb>] ? _raw_spin_unlock_irqrestore+0x3b/0x60
[<ffffffff8148bcea>] ? do_setitimer+0x39a/0x8e0
[<ffffffff813aa9bb>] ? __might_sleep+0x5b/0x260
[<ffffffff833c9110>] ? __sys_recvmmsg+0x790/0x790
[<ffffffff833c91e9>] SyS_recvmmsg+0xd9/0x160
[<ffffffff833c9110>] ? __sys_recvmmsg+0x790/0x790
[<ffffffff823c7853>] ? __this_cpu_preempt_check+0x13/0x20
[<ffffffff8162f680>] ? __context_tracking_exit.part.3+0x30/0x1b0
[<ffffffff833c9110>] ? __sys_recvmmsg+0x790/0x790
[<ffffffff81007bd3>] do_syscall_64+0x1b3/0x4b0
[<ffffffff845f936a>] entry_SYSCALL64_slow_path+0x25/0x25
================================================================================
Line 783 is this:
783 set_normalized_timespec64(&res, lhs.tv_sec + rhs.tv_sec,
784 lhs.tv_nsec + rhs.tv_nsec);
In other words, since lhs.tv_sec and rhs.tv_sec are both time64_t, this
is a signed addition which will cause undefined behaviour on overflow.
Note that this is not currently a huge concern since the kernel should be
built with -fno-strict-overflow by default, but could be a problem in the
future, a problem with older compilers, or other compilers than gcc.
The easiest way to avoid the overflow is to cast one of the arguments to
unsigned (so the addition will be done using unsigned arithmetic).
Cc: Thomas Gleixner <tglx@linutronix.de>
Cc: Ingo Molnar <mingo@kernel.org>
Cc: Richard Cochran <richardcochran@gmail.com>
Cc: Prarit Bhargava <prarit@redhat.com>
Signed-off-by: Vegard Nossum <vegard.nossum@oracle.com>
Signed-off-by: John Stultz <john.stultz@linaro.org>