commit b5740f4b2c upstream.
try_to_wake_up() has a problem which may change status from TASK_DEAD to
TASK_RUNNING in race condition with SMI or guest environment of virtual
machine. As a result, exited task is scheduled() again and panic occurs.
Here is the sequence how it occurs:
----------------------------------+-----------------------------
|
CPU A | CPU B
----------------------------------+-----------------------------
TASK A calls exit()....
do_exit()
exit_mm()
down_read(mm->mmap_sem);
rwsem_down_failed_common()
set TASK_UNINTERRUPTIBLE
set waiter.task <= task A
list_add to sem->wait_list
:
raw_spin_unlock_irq()
(I/O interruption occured)
__rwsem_do_wake(mmap_sem)
list_del(&waiter->list);
waiter->task = NULL
wake_up_process(task A)
try_to_wake_up()
(task is still
TASK_UNINTERRUPTIBLE)
p->on_rq is still 1.)
ttwu_do_wakeup()
(*A)
:
(I/O interruption handler finished)
if (!waiter.task)
schedule() is not called
due to waiter.task is NULL.
tsk->state = TASK_RUNNING
:
check_preempt_curr();
:
task->state = TASK_DEAD
(*B)
<--- set TASK_RUNNING (*C)
schedule()
(exit task is running again)
BUG_ON() is called!
--------------------------------------------------------
The execution time between (*A) and (*B) is usually very short,
because the interruption is disabled, and setting TASK_RUNNING at (*C)
must be executed before setting TASK_DEAD.
HOWEVER, if SMI is interrupted between (*A) and (*B),
(*C) is able to execute AFTER setting TASK_DEAD!
Then, exited task is scheduled again, and BUG_ON() is called....
If the system works on guest system of virtual machine, the time
between (*A) and (*B) may be also long due to scheduling of hypervisor,
and same phenomenon can occur.
By this patch, do_exit() waits for releasing task->pi_lock which is used
in try_to_wake_up(). It guarantees the task becomes TASK_DEAD after
waking up.
Signed-off-by: Yasunori Goto <y-goto@jp.fujitsu.com>
Acked-by: Oleg Nesterov <oleg@redhat.com>
Signed-off-by: Peter Zijlstra <a.p.zijlstra@chello.nl>
Cc: Linus Torvalds <torvalds@linux-foundation.org>
Cc: Andrew Morton <akpm@linux-foundation.org>
Link: http://lkml.kernel.org/r/20120117174031.3118.E1E9C6FF@jp.fujitsu.com
Signed-off-by: Ingo Molnar <mingo@elte.hu>
Cc: Michal Hocko <mhocko@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit cee58483cf upstream
Andreas Bombe reported that the added ktime_t overflow checking added to
timespec_valid in commit 4e8b14526c ("time: Improve sanity checking of
timekeeping inputs") was causing problems with X.org because it caused
timeouts larger then KTIME_T to be invalid.
Previously, these large timeouts would be clamped to KTIME_MAX and would
never expire, which is valid.
This patch splits the ktime_t overflow checking into a new
timespec_valid_strict function, and converts the timekeeping codes
internal checking to use this more strict function.
Reported-and-tested-by: Andreas Bombe <aeb@debian.org>
Cc: Zhouping Liu <zliu@redhat.com>
Cc: Ingo Molnar <mingo@kernel.org>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: John Stultz <john.stultz@linaro.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: John Stultz <john.stultz@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 4e8b14526c upstream
Unexpected behavior could occur if the time is set to a value large
enough to overflow a 64bit ktime_t (which is something larger then the
year 2262).
Also unexpected behavior could occur if large negative offsets are
injected via adjtimex.
So this patch improves the sanity check timekeeping inputs by
improving the timespec_valid() check, and then makes better use of
timespec_valid() to make sure we don't set the time to an invalid
negative value or one that overflows ktime_t.
Note: This does not protect from setting the time close to overflowing
ktime_t and then letting natural accumulation cause the overflow.
Reported-by: CAI Qian <caiqian@redhat.com>
Reported-by: Sasha Levin <levinsasha928@gmail.com>
Signed-off-by: John Stultz <john.stultz@linaro.org>
Cc: Peter Zijlstra <a.p.zijlstra@chello.nl>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Zhouping Liu <zliu@redhat.com>
Cc: Ingo Molnar <mingo@kernel.org>
Link: http://lkml.kernel.org/r/1344454580-17031-1-git-send-email-john.stultz@linaro.org
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: John Stultz <john.stultz@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 8323f26ce3 upstream.
Stefan reported a crash on a kernel before a3e5d1091c ("sched:
Don't call task_group() too many times in set_task_rq()"), he
found the reason to be that the multiple task_group()
invocations in set_task_rq() returned different values.
Looking at all that I found a lack of serialization and plain
wrong comments.
The below tries to fix it using an extra pointer which is
updated under the appropriate scheduler locks. Its not pretty,
but I can't really see another way given how all the cgroup
stuff works.
Reported-and-tested-by: Stefan Bader <stefan.bader@canonical.com>
Signed-off-by: Peter Zijlstra <a.p.zijlstra@chello.nl>
Link: http://lkml.kernel.org/r/1340364965.18025.71.camel@twins
Signed-off-by: Ingo Molnar <mingo@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[Fixed upstream by commits 2955b47d2c and
a4683487f9 from Dan Williams, but they are much
more intrusive than this tiny fix, according to Andrew - gregkh]
This patch tries to fix a dead loop in async_synchronize_full(), which
could be seen when preemption is disabled on a single cpu machine.
void async_synchronize_full(void)
{
do {
async_synchronize_cookie(next_cookie);
} while (!list_empty(&async_running) || !
list_empty(&async_pending));
}
async_synchronize_cookie() calls async_synchronize_cookie_domain() with
&async_running as the default domain to synchronize.
However, there might be some works in the async_pending list from other
domains. On a single cpu system, without preemption, there is no chance
for the other works to finish, so async_synchronize_full() enters a dead
loop.
It seems async_synchronize_full() wants to synchronize all entries in
all running lists(domains), so maybe we could just check the entry_count
to know whether all works are finished.
Currently, async_synchronize_cookie_domain() expects a non-NULL running
list ( if NULL, there would be NULL pointer dereference ), so maybe a
NULL pointer could be used as an indication for the functions to
synchronize all works in all domains.
Reported-by: Paul E. McKenney <paulmck@linux.vnet.ibm.com>
Signed-off-by: Li Zhong <zhong@linux.vnet.ibm.com>
Tested-by: Paul E. McKenney <paulmck@linux.vnet.ibm.com>
Tested-by: Christian Kujau <lists@nerdbynature.de>
Cc: Andrew Morton <akpm@linux-foundation.org>
Cc: Dan Williams <dan.j.williams@gmail.com>
Cc: Christian Kujau <lists@nerdbynature.de>
Cc: Andrew Morton <akpm@linux-foundation.org>
Cc: Cong Wang <xiyou.wangcong@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 96e65306b8 upstream.
The compiler may compile the following code into TWO write/modify
instructions.
worker->flags &= ~WORKER_UNBOUND;
worker->flags |= WORKER_REBIND;
so the other CPU may temporarily see worker->flags which doesn't have
either WORKER_UNBOUND or WORKER_REBIND set and perform local wakeup
prematurely.
Fix it by using single explicit assignment via ACCESS_ONCE().
Because idle workers have another WORKER_NOT_RUNNING flag, this bug
doesn't exist for them; however, update it to use the same pattern for
consistency.
tj: Applied the change to idle workers too and updated comments and
patch description a bit.
Signed-off-by: Lai Jiangshan <laijs@cn.fujitsu.com>
Signed-off-by: Tejun Heo <tj@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit a6fa941d94 upstream.
Don't mess with file refcounts (or keep a reference to file, for
that matter) in perf_event. Use explicit refcount of its own
instead. Deal with the race between the final reference to event
going away and new children getting created for it by use of
atomic_long_inc_not_zero() in inherit_event(); just have the
latter free what it had allocated and return NULL, that works
out just fine (children of siblings of something doomed are
created as singletons, same as if the child of leader had been
created and immediately killed).
Signed-off-by: Al Viro <viro@zeniv.linux.org.uk>
Signed-off-by: Peter Zijlstra <a.p.zijlstra@chello.nl>
Link: http://lkml.kernel.org/r/20120820135925.GG23464@ZenIV.linux.org.uk
Signed-off-by: Ingo Molnar <mingo@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit ed48ece27c upstream.
The existing work_on_cpu() implementation is hugely inefficient. It
creates a new kthread, execute that single function and then let the
kthread die on each invocation.
Now that system_wq can handle concurrent executions, there's no
advantage of doing this. Reimplement work_on_cpu() using system_wq
which makes it simpler and way more efficient.
stable: While this isn't a fix in itself, it's needed to fix a
workqueue related bug in cpufreq/powernow-k8. AFAICS, this
shouldn't break other existing users.
Signed-off-by: Tejun Heo <tj@kernel.org>
Acked-by: Jiri Kosina <jkosina@suse.cz>
Cc: Linus Torvalds <torvalds@linux-foundation.org>
Cc: Bjorn Helgaas <bhelgaas@google.com>
Cc: Len Brown <lenb@kernel.org>
Cc: Rafael J. Wysocki <rjw@sisk.pl>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit a2140fc0cb upstream.
Refcounting of fsnotify_mark in audit tree is broken. E.g:
refcount
create_chunk
alloc_chunk 1
fsnotify_add_mark 2
untag_chunk
fsnotify_get_mark 3
fsnotify_destroy_mark
audit_tree_freeing_mark 2
fsnotify_put_mark 1
fsnotify_put_mark 0
via destroy_list
fsnotify_mark_destroy -1
This was reported by various people as triggering Oops when stopping auditd.
We could just remove the put_mark from audit_tree_freeing_mark() but that would
break freeing via inode destruction. So this patch simply omits a put_mark
after calling destroy_mark or adds a get_mark before.
The additional get_mark is necessary where there's no other put_mark after
fsnotify_destroy_mark() since it assumes that the caller is holding a reference
(or the inode is keeping the mark pinned, not the case here AFAICS).
Signed-off-by: Miklos Szeredi <mszeredi@suse.cz>
Reported-by: Valentin Avram <aval13@gmail.com>
Reported-by: Peter Moody <pmoody@google.com>
Acked-by: Eric Paris <eparis@redhat.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 0fe33aae0e upstream.
Don't do free_chunk() after fsnotify_add_mark(). That one does a delayed unref
via the destroy list and this results in use-after-free.
Signed-off-by: Miklos Szeredi <mszeredi@suse.cz>
Acked-by: Eric Paris <eparis@redhat.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit c5857ccf29 upstream.
With the new interrupt sampling system, we are no longer using the
timer_rand_state structure in the irq descriptor, so we can stop
initializing it now.
[ Merged in fixes from Sedat to find some last missing references to
rand_initialize_irq() ]
Signed-off-by: "Theodore Ts'o" <tytso@mit.edu>
Signed-off-by: Sedat Dilek <sedat.dilek@gmail.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 775f4b297b upstream.
We've been moving away from add_interrupt_randomness() for various
reasons: it's too expensive to do on every interrupt, and flooding the
CPU with interrupts could theoretically cause bogus floods of entropy
from a somewhat externally controllable source.
This solves both problems by limiting the actual randomness addition
to just once a second or after 64 interrupts, whicever comes first.
During that time, the interrupt cycle data is buffered up in a per-cpu
pool. Also, we make sure the the nonblocking pool used by urandom is
initialized before we start feeding the normal input pool. This
assures that /dev/urandom is returning unpredictable data as soon as
possible.
(Based on an original patch by Linus, but significantly modified by
tytso.)
Tested-by: Eric Wustrow <ewust@umich.edu>
Reported-by: Eric Wustrow <ewust@umich.edu>
Reported-by: Nadia Heninger <nadiah@cs.ucsd.edu>
Reported-by: Zakir Durumeric <zakir@umich.edu>
Reported-by: J. Alex Halderman <jhalderm@umich.edu>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: "Theodore Ts'o" <tytso@mit.edu>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 6575820221 upstream.
Currently, all workqueue cpu hotplug operations run off
CPU_PRI_WORKQUEUE which is higher than normal notifiers. This is to
ensure that workqueue is up and running while bringing up a CPU before
other notifiers try to use workqueue on the CPU.
Per-cpu workqueues are supposed to remain working and bound to the CPU
for normal CPU_DOWN_PREPARE notifiers. This holds mostly true even
with workqueue offlining running with higher priority because
workqueue CPU_DOWN_PREPARE only creates a bound trustee thread which
runs the per-cpu workqueue without concurrency management without
explicitly detaching the existing workers.
However, if the trustee needs to create new workers, it creates
unbound workers which may wander off to other CPUs while
CPU_DOWN_PREPARE notifiers are in progress. Furthermore, if the CPU
down is cancelled, the per-CPU workqueue may end up with workers which
aren't bound to the CPU.
While reliably reproducible with a convoluted artificial test-case
involving scheduling and flushing CPU burning work items from CPU down
notifiers, this isn't very likely to happen in the wild, and, even
when it happens, the effects are likely to be hidden by the following
successful CPU down.
Fix it by using different priorities for up and down notifiers - high
priority for up operations and low priority for down operations.
Workqueue cpu hotplug operations will soon go through further cleanup.
Signed-off-by: Tejun Heo <tj@kernel.org>
Acked-by: "Rafael J. Wysocki" <rjw@sisk.pl>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 443772d408 upstream.
If function tracing is enabled for some of the low-level suspend/resume
functions, it leads to triple fault during resume from suspend, ultimately
ending up in a reboot instead of a resume (or a total refusal to come out
of suspended state, on some machines).
This issue was explained in more detail in commit f42ac38c59 (ftrace:
disable tracing for suspend to ram). However, the changes made by that commit
got reverted by commit cbe2f5a6e8 (tracing: allow tracing of
suspend/resume & hibernation code again). So, unfortunately since things are
not yet robust enough to allow tracing of low-level suspend/resume functions,
suspend/resume is still broken when ftrace is enabled.
So fix this by disabling function tracing during suspend/resume & hibernation.
Signed-off-by: Srivatsa S. Bhat <srivatsa.bhat@linux.vnet.ibm.com>
Signed-off-by: Rafael J. Wysocki <rjw@sisk.pl>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit cc9a6c8776 upstream.
Stable note: Not tracked in Bugzilla. [get|put]_mems_allowed() is extremely
expensive and severely impacted page allocator performance. This
is part of a series of patches that reduce page allocator overhead.
Commit c0ff7453bb ("cpuset,mm: fix no node to alloc memory when
changing cpuset's mems") wins a super prize for the largest number of
memory barriers entered into fast paths for one commit.
[get|put]_mems_allowed is incredibly heavy with pairs of full memory
barriers inserted into a number of hot paths. This was detected while
investigating at large page allocator slowdown introduced some time
after 2.6.32. The largest portion of this overhead was shown by
oprofile to be at an mfence introduced by this commit into the page
allocator hot path.
For extra style points, the commit introduced the use of yield() in an
implementation of what looks like a spinning mutex.
This patch replaces the full memory barriers on both read and write
sides with a sequence counter with just read barriers on the fast path
side. This is much cheaper on some architectures, including x86. The
main bulk of the patch is the retry logic if the nodemask changes in a
manner that can cause a false failure.
While updating the nodemask, a check is made to see if a false failure
is a risk. If it is, the sequence number gets bumped and parallel
allocators will briefly stall while the nodemask update takes place.
In a page fault test microbenchmark, oprofile samples from
__alloc_pages_nodemask went from 4.53% of all samples to 1.15%. The
actual results were
3.3.0-rc3 3.3.0-rc3
rc3-vanilla nobarrier-v2r1
Clients 1 UserTime 0.07 ( 0.00%) 0.08 (-14.19%)
Clients 2 UserTime 0.07 ( 0.00%) 0.07 ( 2.72%)
Clients 4 UserTime 0.08 ( 0.00%) 0.07 ( 3.29%)
Clients 1 SysTime 0.70 ( 0.00%) 0.65 ( 6.65%)
Clients 2 SysTime 0.85 ( 0.00%) 0.82 ( 3.65%)
Clients 4 SysTime 1.41 ( 0.00%) 1.41 ( 0.32%)
Clients 1 WallTime 0.77 ( 0.00%) 0.74 ( 4.19%)
Clients 2 WallTime 0.47 ( 0.00%) 0.45 ( 3.73%)
Clients 4 WallTime 0.38 ( 0.00%) 0.37 ( 1.58%)
Clients 1 Flt/sec/cpu 497620.28 ( 0.00%) 520294.53 ( 4.56%)
Clients 2 Flt/sec/cpu 414639.05 ( 0.00%) 429882.01 ( 3.68%)
Clients 4 Flt/sec/cpu 257959.16 ( 0.00%) 258761.48 ( 0.31%)
Clients 1 Flt/sec 495161.39 ( 0.00%) 517292.87 ( 4.47%)
Clients 2 Flt/sec 820325.95 ( 0.00%) 850289.77 ( 3.65%)
Clients 4 Flt/sec 1020068.93 ( 0.00%) 1022674.06 ( 0.26%)
MMTests Statistics: duration
Sys Time Running Test (seconds) 135.68 132.17
User+Sys Time Running Test (seconds) 164.2 160.13
Total Elapsed Time (seconds) 123.46 120.87
The overall improvement is small but the System CPU time is much
improved and roughly in correlation to what oprofile reported (these
performance figures are without profiling so skew is expected). The
actual number of page faults is noticeably improved.
For benchmarks like kernel builds, the overall benefit is marginal but
the system CPU time is slightly reduced.
To test the actual bug the commit fixed I opened two terminals. The
first ran within a cpuset and continually ran a small program that
faulted 100M of anonymous data. In a second window, the nodemask of the
cpuset was continually randomised in a loop.
Without the commit, the program would fail every so often (usually
within 10 seconds) and obviously with the commit everything worked fine.
With this patch applied, it also worked fine so the fix should be
functionally equivalent.
Signed-off-by: Mel Gorman <mgorman@suse.de>
Cc: Miao Xie <miaox@cn.fujitsu.com>
Cc: David Rientjes <rientjes@google.com>
Cc: Peter Zijlstra <a.p.zijlstra@chello.nl>
Cc: Christoph Lameter <cl@linux.com>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: Mel Gorman <mgorman@suse.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit b246272ecc upstream.
Stable note: Not tracked in Bugzilla. [get|put]_mems_allowed() is extremely
expensive and severely impacted page allocator performance. This is
part of a series of patches that reduce page allocator overhead.
Kernels where MAX_NUMNODES > BITS_PER_LONG may temporarily see an empty
nodemask in a tsk's mempolicy if its previous nodemask is remapped onto a
new set of allowed cpuset nodes where the two nodemasks, as a result of
the remap, are now disjoint.
c0ff7453bb ("cpuset,mm: fix no node to alloc memory when changing
cpuset's mems") adds get_mems_allowed() to prevent the set of allowed
nodes from changing for a thread. This causes any update to a set of
allowed nodes to stall until put_mems_allowed() is called.
This stall is unncessary, however, if at least one node remains unchanged
in the update to the set of allowed nodes. This was addressed by
89e8a244b9 ("cpusets: avoid looping when storing to mems_allowed if one
node remains set"), but it's still possible that an empty nodemask may be
read from a mempolicy because the old nodemask may be remapped to the new
nodemask during rebind. To prevent this, only avoid the stall if there is
no mempolicy for the thread being changed.
This is a temporary solution until all reads from mempolicy nodemasks can
be guaranteed to not be empty without the get_mems_allowed()
synchronization.
Also moves the check for nodemask intersection inside task_lock() so that
tsk->mems_allowed cannot change. This ensures that nothing can set this
tsk's mems_allowed out from under us and also protects tsk->mempolicy.
Reported-by: Miao Xie <miaox@cn.fujitsu.com>
Signed-off-by: David Rientjes <rientjes@google.com>
Cc: KOSAKI Motohiro <kosaki.motohiro@jp.fujitsu.com>
Cc: Paul Menage <paul@paulmenage.org>
Cc: Stephen Rothwell <sfr@canb.auug.org.au>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: Mel Gorman <mgorman@suse.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 89e8a244b9 upstream.
Stable note: Not tracked in Bugzilla. [get|put]_mems_allowed() is
extremely expensive and severely impacted page allocator performance.
This is part of a series of patches that reduce page allocator
overhead.
{get,put}_mems_allowed() exist so that general kernel code may locklessly
access a task's set of allowable nodes without having the chance that a
concurrent write will cause the nodemask to be empty on configurations
where MAX_NUMNODES > BITS_PER_LONG.
This could incur a significant delay, however, especially in low memory
conditions because the page allocator is blocking and reclaim requires
get_mems_allowed() itself. It is not atypical to see writes to
cpuset.mems take over 2 seconds to complete, for example. In low memory
conditions, this is problematic because it's one of the most imporant
times to change cpuset.mems in the first place!
The only way a task's set of allowable nodes may change is through cpusets
by writing to cpuset.mems and when attaching a task to a generic code is
not reading the nodemask with get_mems_allowed() at the same time, and
then clearing all the old nodes. This prevents the possibility that a
reader will see an empty nodemask at the same time the writer is storing a
new nodemask.
If at least one node remains unchanged, though, it's possible to simply
set all new nodes and then clear all the old nodes. Changing a task's
nodemask is protected by cgroup_mutex so it's guaranteed that two threads
are not changing the same task's nodemask at the same time, so the
nodemask is guaranteed to be stored before another thread changes it and
determines whether a node remains set or not.
Signed-off-by: David Rientjes <rientjes@google.com>
Cc: Miao Xie <miaox@cn.fujitsu.com>
Cc: KOSAKI Motohiro <kosaki.motohiro@jp.fujitsu.com>
Cc: Nick Piggin <npiggin@kernel.dk>
Cc: Paul Menage <paul@paulmenage.org>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: Mel Gorman <mgorman@suse.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is a backport of 3e997130bd
The leap second rework unearthed another issue of inconsistent data.
On timekeeping_resume() the timekeeper data is updated, but nothing
calls timekeeping_update(), so now the update code in the timer
interrupt sees stale values.
This has been the case before those changes, but then the timer
interrupt was using stale data as well so this went unnoticed for quite
some time.
Add the missing update call, so all the data is consistent everywhere.
Reported-by: Andreas Schwab <schwab@linux-m68k.org>
Reported-and-tested-by: "Rafael J. Wysocki" <rjw@sisk.pl>
Reported-and-tested-by: Martin Steigerwald <Martin@lichtvoll.de>
Cc: John Stultz <johnstul@us.ibm.com>
Cc: Ingo Molnar <mingo@kernel.org>
Cc: Peter Zijlstra <a.p.zijlstra@chello.nl>,
Cc: Prarit Bhargava <prarit@redhat.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: John Stultz <johnstul@us.ibm.com>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: John Stultz <johnstul@us.ibm.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is a backport of 5baefd6d84
The update of the hrtimer base offsets on all cpus cannot be made
atomically from the timekeeper.lock held and interrupt disabled region
as smp function calls are not allowed there.
clock_was_set(), which enforces the update on all cpus, is called
either from preemptible process context in case of do_settimeofday()
or from the softirq context when the offset modification happened in
the timer interrupt itself due to a leap second.
In both cases there is a race window for an hrtimer interrupt between
dropping timekeeper lock, enabling interrupts and clock_was_set()
issuing the updates. Any interrupt which arrives in that window will
see the new time but operate on stale offsets.
So we need to make sure that an hrtimer interrupt always sees a
consistent state of time and offsets.
ktime_get_update_offsets() allows us to get the current monotonic time
and update the per cpu hrtimer base offsets from hrtimer_interrupt()
to capture a consistent state of monotonic time and the offsets. The
function replaces the existing ktime_get() calls in hrtimer_interrupt().
The overhead of the new function vs. ktime_get() is minimal as it just
adds two store operations.
This ensures that any changes to realtime or boottime offsets are
noticed and stored into the per-cpu hrtimer base structures, prior to
any hrtimer expiration and guarantees that timers are not expired early.
Signed-off-by: John Stultz <johnstul@us.ibm.com>
Reviewed-by: Ingo Molnar <mingo@kernel.org>
Acked-by: Peter Zijlstra <a.p.zijlstra@chello.nl>
Acked-by: Prarit Bhargava <prarit@redhat.com>
Link: http://lkml.kernel.org/r/1341960205-56738-8-git-send-email-johnstul@us.ibm.com
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: John Stultz <johnstul@us.ibm.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is a backport of f6c06abfb3
To finally fix the infamous leap second issue and other race windows
caused by functions which change the offsets between the various time
bases (CLOCK_MONOTONIC, CLOCK_REALTIME and CLOCK_BOOTTIME) we need a
function which atomically gets the current monotonic time and updates
the offsets of CLOCK_REALTIME and CLOCK_BOOTTIME with minimalistic
overhead. The previous patch which provides ktime_t offsets allows us
to make this function almost as cheap as ktime_get() which is going to
be replaced in hrtimer_interrupt().
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Reviewed-by: Ingo Molnar <mingo@kernel.org>
Acked-by: Peter Zijlstra <a.p.zijlstra@chello.nl>
Acked-by: Prarit Bhargava <prarit@redhat.com>
Signed-off-by: John Stultz <johnstul@us.ibm.com>
Link: http://lkml.kernel.org/r/1341960205-56738-7-git-send-email-johnstul@us.ibm.com
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: John Stultz <johnstul@us.ibm.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is a backport of 4873fa070a
The timekeeping code misses an update of the hrtimer subsystem after a
leap second happened. Due to that timers based on CLOCK_REALTIME are
either expiring a second early or late depending on whether a leap
second has been inserted or deleted until an operation is initiated
which causes that update. Unless the update happens by some other
means this discrepancy between the timekeeping and the hrtimer data
stays forever and timers are expired either early or late.
The reported immediate workaround - $ data -s "`date`" - is causing a
call to clock_was_set() which updates the hrtimer data structures.
See: http://www.sheeri.com/content/mysql-and-leap-second-high-cpu-and-fix
Add the missing clock_was_set() call to update_wall_time() in case of
a leap second event. The actual update is deferred to softirq context
as the necessary smp function call cannot be invoked from hard
interrupt context.
Signed-off-by: John Stultz <johnstul@us.ibm.com>
Reported-by: Jan Engelhardt <jengelh@inai.de>
Reviewed-by: Ingo Molnar <mingo@kernel.org>
Acked-by: Peter Zijlstra <a.p.zijlstra@chello.nl>
Acked-by: Prarit Bhargava <prarit@redhat.com>
Link: http://lkml.kernel.org/r/1341960205-56738-3-git-send-email-johnstul@us.ibm.com
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: John Stultz <johnstul@us.ibm.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is a backport of f55a6faa38
clock_was_set() cannot be called from hard interrupt context because
it calls on_each_cpu().
For fixing the widely reported leap seconds issue it is necessary to
call it from hard interrupt context, i.e. the timer tick code, which
does the timekeeping updates.
Provide a new function which denotes it in the hrtimer cpu base
structure of the cpu on which it is called and raise the hrtimer
softirq. We then execute the clock_was_set() notificiation from
softirq context in run_hrtimer_softirq(). The hrtimer softirq is
rarely used, so polling the flag there is not a performance issue.
[ tglx: Made it depend on CONFIG_HIGH_RES_TIMERS. We really should get
rid of all this ifdeffery ASAP ]
Signed-off-by: John Stultz <johnstul@us.ibm.com>
Reported-by: Jan Engelhardt <jengelh@inai.de>
Reviewed-by: Ingo Molnar <mingo@kernel.org>
Acked-by: Peter Zijlstra <a.p.zijlstra@chello.nl>
Acked-by: Prarit Bhargava <prarit@redhat.com>
Link: http://lkml.kernel.org/r/1341960205-56738-2-git-send-email-johnstul@us.ibm.com
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: John Stultz <johnstul@us.ibm.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is a backport of dd48d708ff
When repeating a UTC time value during a leap second (when the UTC
time should be 23:59:60), the TAI timescale should not stop. The kernel
NTP code increments the TAI offset one second too late. This patch fixes
the issue by incrementing the offset during the leap second itself.
Signed-off-by: Richard Cochran <richardcochran@gmail.com>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: John Stultz <john.stultz@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This is a backport of 6b43ae8a61
This should have been backported when it was commited, but I
mistook the problem as requiring the ntp_lock changes
that landed in 3.4 in order for it to occur.
Unfortunately the same issue can happen (with only one cpu)
as follows:
do_adjtimex()
write_seqlock_irq(&xtime_lock);
process_adjtimex_modes()
process_adj_status()
ntp_start_leap_timer()
hrtimer_start()
hrtimer_reprogram()
tick_program_event()
clockevents_program_event()
ktime_get()
seq = req_seqbegin(xtime_lock); [DEADLOCK]
This deadlock will no always occur, as it requires the
leap_timer to force a hrtimer_reprogram which only happens
if its set and there's no sooner timer to expire.
NOTE: This patch, being faithful to the original commit,
introduces a bug (we don't update wall_to_monotonic),
which will be resovled by backporting a following fix.
Original commit message below:
Since commit 7dffa3c673 the ntp
subsystem has used an hrtimer for triggering the leapsecond
adjustment. However, this can cause a potential livelock.
Thomas diagnosed this as the following pattern:
CPU 0 CPU 1
do_adjtimex()
spin_lock_irq(&ntp_lock);
process_adjtimex_modes(); timer_interrupt()
process_adj_status(); do_timer()
ntp_start_leap_timer(); write_lock(&xtime_lock);
hrtimer_start(); update_wall_time();
hrtimer_reprogram(); ntp_tick_length()
tick_program_event() spin_lock(&ntp_lock);
clockevents_program_event()
ktime_get()
seq = req_seqbegin(xtime_lock);
This patch tries to avoid the problem by reverting back to not using
an hrtimer to inject leapseconds, and instead we handle the leapsecond
processing in the second_overflow() function.
The downside to this change is that on systems that support highres
timers, the leap second processing will occur on a HZ tick boundary,
(ie: ~1-10ms, depending on HZ) after the leap second instead of
possibly sooner (~34us in my tests w/ x86_64 lapic).
This patch applies on top of tip/timers/core.
CC: Sasha Levin <levinsasha928@gmail.com>
CC: Thomas Gleixner <tglx@linutronix.de>
Reported-by: Sasha Levin <levinsasha928@gmail.com>
Diagnoised-by: Thomas Gleixner <tglx@linutronix.de>
Tested-by: Sasha Levin <levinsasha928@gmail.com>
Cc: Prarit Bhargava <prarit@redhat.com>
Cc: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: John Stultz <john.stultz@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit a841f8cef4 upstream.
It does not get processed because sched_domain_level_max is 0 at the
time that setup_relax_domain_level() is run.
Simply accept the value as it is, as we don't know the value of
sched_domain_level_max until sched domain construction is completed.
Fix sched_relax_domain_level in cpuset. The build_sched_domain() routine calls
the set_domain_attribute() routine prior to setting the sd->level, however,
the set_domain_attribute() routine relies on the sd->level to decide whether
idle load balancing will be off/on.
Signed-off-by: Dimitri Sivanich <sivanich@sgi.com>
Signed-off-by: Peter Zijlstra <a.p.zijlstra@chello.nl>
Link: http://lkml.kernel.org/r/20120605184436.GA15668@sgi.com
Signed-off-by: Ingo Molnar <mingo@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 544ecf310f upstream.
worker_enter_idle() has WARN_ON_ONCE() which triggers if nr_running
isn't zero when every worker is idle. This can trigger spuriously
while a cpu is going down due to the way trustee sets %WORKER_ROGUE
and zaps nr_running.
It first sets %WORKER_ROGUE on all workers without updating
nr_running, releases gcwq->lock, schedules, regrabs gcwq->lock and
then zaps nr_running. If the last running worker enters idle
inbetween, it would see stale nr_running which hasn't been zapped yet
and trigger the WARN_ON_ONCE().
Fix it by performing the sanity check iff the trustee is idle.
Signed-off-by: Tejun Heo <tj@kernel.org>
Reported-by: "Paul E. McKenney" <paulmck@linux.vnet.ibm.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit b7dafa0ef3 upstream.
compat_sys_sigprocmask reads a smaller signal mask from userspace than
sigprogmask accepts for setting. So the high word of blocked.sig[0]
will be cleared, releasing any potentially blocked RT signal.
This was discovered via userspace code that relies on get/setcontext.
glibc's i386 versions of those functions use sigprogmask instead of
rt_sigprogmask to save/restore signal mask and caused RT signal
unblocking this way.
As suggested by Linus, this replaces the sys_sigprocmask based compat
version with one that open-codes the required logic, including the merge
of the existing blocked set with the new one provided on SIG_SETMASK.
Signed-off-by: Jan Kiszka <jan.kiszka@siemens.com>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 6f103929f8 upstream.
Fix tick_nohz_restart() to not use a stale ktime_t "now" value when
calling tick_do_update_jiffies64(now).
If we reach this point in the loop it means that we crossed a tick
boundary since we grabbed the "now" timestamp, so at this point "now"
refers to a time in the old jiffy, so using the old value for "now" is
incorrect, and is likely to give us a stale jiffies value.
In particular, the first time through the loop the
tick_do_update_jiffies64(now) call is always a no-op, since the
caller, tick_nohz_restart_sched_tick(), will have already called
tick_do_update_jiffies64(now) with that "now" value.
Note that tick_nohz_stop_sched_tick() already uses the correct
approach: when we notice we cross a jiffy boundary, grab a new
timestamp with ktime_get(), and *then* update jiffies.
Signed-off-by: Neal Cardwell <ncardwell@google.com>
Cc: Ben Segall <bsegall@google.com>
Cc: Ingo Molnar <mingo@elte.hu>
Link: http://lkml.kernel.org/r/1332875377-23014-1-git-send-email-ncardwell@google.com
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 79549c6dfd upstream.
keyctl_session_to_parent(task) sets ->replacement_session_keyring,
it should be processed and cleared by key_replace_session_keyring().
However, this task can fork before it notices TIF_NOTIFY_RESUME and
the new child gets the bogus ->replacement_session_keyring copied by
dup_task_struct(). This is obviously wrong and, if nothing else, this
leads to put_cred(already_freed_cred).
change copy_creds() to clear this member. If copy_process() fails
before this point the wrong ->replacement_session_keyring doesn't
matter, exit_creds() won't be called.
Signed-off-by: Oleg Nesterov <oleg@redhat.com>
Acked-by: David Howells <dhowells@redhat.com>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 620f6e8e85 upstream.
Commit bfdc0b4 adds code to restrict access to dmesg_restrict,
however, it incorrectly alters kptr_restrict rather than
dmesg_restrict.
The original patch from Richard Weinberger
(https://lkml.org/lkml/2011/3/14/362) alters dmesg_restrict as
expected, and so the patch seems to have been misapplied.
This adds the CAP_SYS_ADMIN check to both dmesg_restrict and
kptr_restrict, since both are sensitive.
Reported-by: Phillip Lougher <plougher@redhat.com>
Signed-off-by: Kees Cook <keescook@chromium.org>
Acked-by: Serge Hallyn <serge.hallyn@canonical.com>
Acked-by: Richard Weinberger <richard@nod.at>
Signed-off-by: James Morris <james.l.morris@oracle.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 98b54aa1a2 upstream.
There is extra state information that needs to be exposed in the
kgdb_bpt structure for tracking how a breakpoint was installed. The
debug_core only uses the the probe_kernel_write() to install
breakpoints, but this is not enough for all the archs. Some arch such
as x86 need to use text_poke() in order to install a breakpoint into a
read only page.
Passing the kgdb_bpt structure to kgdb_arch_set_breakpoint() and
kgdb_arch_remove_breakpoint() allows other archs to set the type
variable which indicates how the breakpoint was installed.
Signed-off-by: Jason Wessel <jason.wessel@windriver.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit f5cb92ac82 upstream.
irq_move_masked_irq() checks the return code of
chip->irq_set_affinity() only for 0, but IRQ_SET_MASK_OK_NOCOPY is
also a valid return code, which is there to avoid a redundant copy of
the cpumask. But in case of IRQ_SET_MASK_OK_NOCOPY we not only avoid
the redundant copy, we also fail to adjust the thread affinity of an
eventually threaded interrupt handler.
Handle IRQ_SET_MASK_OK (==0) and IRQ_SET_MASK_OK_NOCOPY(==1) return
values correctly by checking the valid return values seperately.
Signed-off-by: Jiang Liu <jiang.liu@huawei.com>
Cc: Jiang Liu <liuj97@gmail.com>
Cc: Keping Chen <chenkeping@huawei.com>
Link: http://lkml.kernel.org/r/1333120296-13563-2-git-send-email-jiang.liu@huawei.com
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit f946eeb931 upstream.
Module size was limited to 64MB, this was legacy limitation due to vmalloc()
which was removed a while ago.
Limiting module size to 64MB is both pointless and affects real world use
cases.
Cc: Tim Abbott <tim.abbott@oracle.com>
Signed-off-by: Sasha Levin <sasha.levin@oracle.com>
Signed-off-by: Rusty Russell <rusty@rustcorp.com.au>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 05b4877f6a upstream.
If create_basic_memory_bitmaps() fails, usermodehelpers are not re-enabled
before returning. Fix this. And while at it, reword the goto labels so that
they look more meaningful.
Signed-off-by: Srivatsa S. Bhat <srivatsa.bhat@linux.vnet.ibm.com>
Signed-off-by: Rafael J. Wysocki <rjw@sisk.pl>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit a09b659cd6 upstream.
In 2008, commit 0c5d1eb77a ("genirq: record trigger type") modified the
way set_irq_type() handles the 'no trigger' condition. However, this has
an adverse effect on PCMCIA support on Intel StrongARM and probably PXA
platforms.
PCMCIA has several status signals on the socket which can trigger
interrupts; some of these status signals depend on the card's mode
(whether it is configured in memory or IO mode). For example, cards have
a 'Ready/IRQ' signal: in memory mode, this provides an indication to
PCMCIA that the card has finished its power up initialization. In IO
mode, it provides the device interrupt signal. Other status signals
switch between on-board battery status and loud speaker output.
In classical PCMCIA implementations, where you have a specific socket
controller, the controller provides a method to mask interrupts from the
socket, and importantly ignore any state transitions on the pins which
correspond with interrupts once masked. This masking prevents unwanted
events caused by the removal and application of socket power being
forwarded.
However, on platforms where there is no socket controller, the PCMCIA
status and interrupt signals are routed to standard edge-triggered GPIOs.
These GPIOs can be configured to interrupt on rising edge, falling edge,
or never. This is where the problems start.
Edge triggered interrupts are required to record events while disabled via
the usual methods of {free,request,disable,enable}_irq() to prevent
problems with dropped interrupts (eg, the 8390 driver uses disable_irq()
to defer the delivery of interrupts). As a result, these interfaces can
not be used to implement the desired behaviour.
The side effect of this is that if the 'Ready/IRQ' GPIO is disabled via
disable_irq() on suspend, and enabled via enable_irq() after resume, we
will record the state transitions caused by powering events as valid
interrupts, and foward them to the card driver, which may attempt to
access a card which is not powered up.
This leads delays resume while drivers spin in their interrupt handlers,
and complaints from drivers before they realize what's happened.
Moreover, in the case of the 'Ready/IRQ' signal, this is requested and
freed by the card driver itself; the PCMCIA core has no idea whether the
interrupt is requested, and, therefore, whether a call to disable_irq()
would be valid. (We tried this around 2.4.17 / 2.5.1 kernel era, and
ended up throwing it out because of this problem.)
Therefore, it was decided back in around 2002 to disable the edge
triggering instead, resulting in all state transitions on the GPIO being
ignored. That's what we actually need the hardware to do.
The commit above changes this behaviour; it explicitly prevents the 'no
trigger' state being selected.
The reason that request_irq() does not accept the 'no trigger' state is
for compatibility with existing drivers which do not provide their desired
triggering configuration. The set_irq_type() function is 'new' and not
used by non-trigger aware drivers.
Therefore, revert this change, and restore previously working platforms
back to their former state.
Signed-off-by: Russell King <rmk+kernel@arm.linux.org.uk>
Cc: linux@arm.linux.org.uk
Cc: Ingo Molnar <mingo@elte.hu>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>