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ARM: dts: LogicPD Torpedo: Fix I2C1 pinmux
commit74402055a2upstream. The pinmuxing was missing for I2C1 which was causing intermittent issues with the PMIC which is connected to I2C1. The bootloader did not quite configure the I2C1 either, so when running at 2.6MHz, it was generating errors at time. This correctly sets the I2C1 pinmuxing so it can operate at 2.6MHz Fixes:687c276761("ARM: dts: Add minimal support for LogicPD Torpedo DM3730 devkit") Signed-off-by: Adam Ford <aford173@gmail.com> Signed-off-by: Tony Lindgren <tony@atomide.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
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committed by
Greg Kroah-Hartman
parent
036c4bdd66
commit
29b2031139
@@ -90,6 +90,8 @@
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};
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&i2c1 {
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pinctrl-names = "default";
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pinctrl-0 = <&i2c1_pins>;
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clock-frequency = <2600000>;
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twl: twl@48 {
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@@ -137,6 +139,12 @@
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OMAP3_CORE1_IOPAD(0x218e, PIN_OUTPUT | MUX_MODE4) /* mcbsp1_fsr.gpio_157 */
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>;
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};
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i2c1_pins: pinmux_i2c1_pins {
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pinctrl-single,pins = <
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OMAP3_CORE1_IOPAD(0x21ba, PIN_INPUT | MUX_MODE0) /* i2c1_scl.i2c1_scl */
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OMAP3_CORE1_IOPAD(0x21bc, PIN_INPUT | MUX_MODE0) /* i2c1_sda.i2c1_sda */
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>;
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};
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};
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&omap3_pmx_core2 {
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