[ Upstream commit 414428c5da ]
A PCI_EJECT message can arrive at the same time we are calling
pci_scan_child_bus() in the workqueue for the previous PCI_BUS_RELATIONS
message or in create_root_hv_pci_bus(). In this case we could potentially
modify the bus from multiple places.
Properly lock the bus access.
Thanks Dexuan Cui <decui@microsoft.com> for pointing out the race condition
in create_root_hv_pci_bus().
Reported-by: Xiaofeng Wang <xiaofwan@redhat.com>
Signed-off-by: Long Li <longli@microsoft.com>
Signed-off-by: Bjorn Helgaas <bhelgaas@google.com>
Acked-by: K. Y. Srinivasan <kys@microsoft.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit d3a78d8bf7 ]
hv_pci_devices_present() is called in hv_pci_remove() when we remove a PCI
device from the host, e.g., by disabling SR-IOV on a device. In
hv_pci_remove(), the bus is already removed before the call, so we don't
need to rescan the bus in the workqueue scheduled from
hv_pci_devices_present().
By introducing bus state hv_pcibus_removed, we can avoid this situation.
Reported-by: Xiaofeng Wang <xiaofwan@redhat.com>
Signed-off-by: Long Li <longli@microsoft.com>
Signed-off-by: Bjorn Helgaas <bhelgaas@google.com>
Acked-by: K. Y. Srinivasan <kys@microsoft.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit add641e7de ]
after act_csum computes the checksum on skbs carrying GSO TCP/UDP packets,
subsequent segmentation fails because skb_needs_check(skb, true) returns
true. Because of that, skb_warn_bad_offload() is invoked and the following
message is displayed:
WARNING: CPU: 3 PID: 28 at net/core/dev.c:2553 skb_warn_bad_offload+0xf0/0xfd
<...>
[<ffffffff8171f486>] skb_warn_bad_offload+0xf0/0xfd
[<ffffffff8161304c>] __skb_gso_segment+0xec/0x110
[<ffffffff8161340d>] validate_xmit_skb+0x12d/0x2b0
[<ffffffff816135d2>] validate_xmit_skb_list+0x42/0x70
[<ffffffff8163c560>] sch_direct_xmit+0xd0/0x1b0
[<ffffffff8163c760>] __qdisc_run+0x120/0x270
[<ffffffff81613b3d>] __dev_queue_xmit+0x23d/0x690
[<ffffffff81613fa0>] dev_queue_xmit+0x10/0x20
Since GSO is able to compute checksum on individual segments of such skbs,
we can simply skip mangling the packet.
Signed-off-by: Davide Caratti <dcaratti@redhat.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit cf5cd9d448 ]
The driver doesn't have a struct of_device_id table but supported devices
are registered via Device Trees. This is working on the assumption that a
I2C device registered via OF will always match a legacy I2C device ID and
that the MODALIAS reported will always be of the form i2c:<device>.
But this could change in the future so the correct approach is to have an
OF device ID table if the devices are registered via OF.
The compatible strings don't have a vendor prefix because that's how it's
used currently, and changing this will be a Device Tree ABI break.
Signed-off-by: Javier Martinez Canillas <javier@osg.samsung.com>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 0107042768 ]
On systems with a large number of CPUs, running sysrq-<q> can cause
watchdog timeouts. There are two slow sections of code in the sysrq-<q>
path in timer_list.c.
1. print_active_timers() - This function is called by print_cpu() and
contains a slow goto loop. On a machine with hundreds of CPUs, this
loop took approximately 100ms for the first CPU in a NUMA node.
(Subsequent CPUs in the same node ran much quicker.) The total time
to print all of the CPUs is ultimately long enough to trigger the
soft lockup watchdog.
2. print_tickdevice() - This function outputs a large amount of textual
information. This function also took approximately 100ms per CPU.
Since sysrq-<q> is not a performance critical path, there should be no
harm in touching the nmi watchdog in both slow sections above. Touching
it in just one location was insufficient on systems with hundreds of
CPUs as occasional timeouts were still observed during testing.
This issue was observed on an Oracle T7 machine with 128 CPUs, but I
anticipate it may affect other systems with similarly large numbers of
CPUs.
Signed-off-by: Tom Hromatka <tom.hromatka@oracle.com>
Reviewed-by: Rob Gardner <rob.gardner@oracle.com>
Signed-off-by: John Stultz <john.stultz@linaro.org>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 1b8955bc5a ]
The scheduler clock framework may not use the correct timeout for the clock
wrap. This happens when a new clock driver calls sched_clock_register()
after the kernel called sched_clock_postinit(). In this case the clock wrap
timeout is too long thus sched_clock_poll() is called too late and the clock
already wrapped.
On my ARM system the scheduler was no longer scheduling any other task than
the idle task because the sched_clock() wrapped.
Signed-off-by: David Engraf <david.engraf@sysgo.com>
Signed-off-by: John Stultz <john.stultz@linaro.org>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 54449af0e0 ]
After changes to v4l2_clk API introduced in v4.1 by commits a37462b919
'[media] V4L: remove clock name from v4l2_clk API' and 4f528afcfb
'[media] V4L: add CCF support to the v4l2_clk API', ov6650 sensor
stopped responding because v4l2_clk_get(), still called with
depreciated V4L2 clock name "mclk", started to return respective CCF
clock instead of the V4l2 one registered by soc_camera. Fix it by
calling v4l2_clk_get() with NULL clock name.
Created and tested on Amstrad Delta against Linux-4.7-rc3 with
omap1_camera fixes.
Signed-off-by: Janusz Krzysztofik <jmkrzyszt@gmail.com>
Signed-off-by: Guennadi Liakhovetski <g.liakhovetski@gmx.de>
Signed-off-by: Mauro Carvalho Chehab <mchehab@s-opensource.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 66a0d59cdd ]
Following a command abort or device reset, ipr's EH handlers wait for
the commands getting aborted to get sent back from the adapter prior to
returning from the EH handler. This fixes up some cases where the
completion handler was not getting called, which would have resulted in
the EH thread waiting until it timed out, greatly extending EH time.
Signed-off-by: Brian King <brking@linux.vnet.ibm.com>
Reviewed-by: Wendy Xiong <wenxiong@linux.vnet.ibm.com>
Tested-by: Wendy Xiong <wenxiong@linux.vnet.ibm.com>
Signed-off-by: Martin K. Petersen <martin.petersen@oracle.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit bcf54d5385 ]
If the length of the modalias is greater than the buffer size, then the
modalias is truncated. However the untruncated length is returned which
will cause an error. Fix this to return the truncated length. If an error
in the case was desired, then then we should just return -ENOMEM.
The reality is no device will ever have 4KB of compatible strings to hit
this case.
Signed-off-by: Rob Herring <robh@kernel.org>
Cc: Frank Rowand <frowand.list@gmail.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit a3a5129e12 ]
Consider the following situation which has been found in a test setup:
Gateway B has claimed client C and gateway A has the same backbone
network as B. C sends a broad- or multicast to B and directly after
this packet decides to send another packet to A due to a better TQ
value. B will forward the broad-/multicast into the backbone as it is
the responsible gw and after that A will claim C as it has been
chosen by C as the best gateway. If it now happens that A claims C
before it has received the broad-/multicast forwarded by B (due to
backbone topology or due to some delay in B when forwarding the
packet) we get a critical situation: in the current code A will
immediately unclaim C when receiving the multicast due to the
roaming client scenario although the position of C has not changed
in the mesh. If this happens the multi-/broadcast forwarded by B
will be sent back into the mesh by A and we have looping packets
until one of the gateways claims C again.
In order to prevent this, unclaiming of a client due to the roaming
client scenario is only done after a certain time is expired after
the last claim of the client. 100 ms are used here, which should be
slow enough for big backbones and slow gateways but fast enough not
to break the roaming client use case.
Acked-by: Simon Wunderlich <sw@simonwunderlich.de>
Signed-off-by: Andreas Pape <apape@phoenixcontact.com>
[sven@narfation.org: fix conflicts with current version]
Signed-off-by: Sven Eckelmann <sven@narfation.org>
Signed-off-by: Simon Wunderlich <sw@simonwunderlich.de>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit ca260ece6a ]
Make sure to check the number of endpoints to avoid dereferencing a
NULL-pointer or accessing memory beyond the endpoint array should a
malicious device lack the expected endpoints.
Fixes: a1030e92c1 ("[PATCH] zd1211rw: Convert installer CDROM device into WLAN device")
Cc: Daniel Drake <dsd@gentoo.org>
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Kalle Valo <kvalo@codeaurora.org>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 4fd4dd8bff ]
Use MACHINE_FLAG_TOPOLOGY instead of MACHINE_HAS_TOPOLOGY when
clearing the bit that indicates if the machine provides topology
information (and if it should be used). Currently works anyway.
Fixes: 68cc795d19 ("s390/topology: make "topology=off" parameter work")
Signed-off-by: Heiko Carstens <heiko.carstens@de.ibm.com>
Signed-off-by: Martin Schwidefsky <schwidefsky@de.ibm.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit e50728effe ]
The link information exists only on the leading hwfn,
but some of its derivatives [e.g., min/max rate] need to
be configured for each hwfn.
When re-basing the VF link view, use the leading hwfn
information as basis for all existing hwfns to allow
said configurations to stick.
Signed-off-by: Yuval Mintz <Yuval.Mintz@cavium.com>
Signed-off-by: David S. Miller <davem@davemloft.net>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit c2a736b698 ]
The moxart interrupt line flags were not respected in previous
driver: instead of assigning them per-consumer, a fixes mask
was set in the controller.
With the migration to a standard Faraday driver we need to
set up and handle the consumer flags correctly. Also remove
the Moxart-specific flags when switching to using real consumer
flags.
Extend the register window to 0x100 bytes as we may have a few
more registers in there and it doesn't hurt.
Tested-by: Jonas Jensen <jonas.jensen@gmail.com>
Signed-off-by: Jonas Jensen <jonas.jensen@gmail.com>
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Olof Johansson <olof@lixom.net>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 88997e4208 ]
wanted_features is a set of features which have to be enabled if a
hardware allows that.
Currently when a vlan device is created, its wanted_features is set to
current features of its base device.
The problem is that the base device can get new features and they are
not propagated to vlan-s of this device.
If we look at bonding devices, they doesn't have this problem and this
patch suggests to fix this issue by the same way how it works for bonding
devices.
We meet this problem, when we try to create a vlan device over a bonding
device. When a system are booting, real devices require time to be
initialized, so bonding devices created without slaves, then vlan
devices are created and only then ethernet devices are added to the
bonding device. As a result we have vlan devices with disabled
scatter-gather.
* create a bonding device
$ ip link add bond0 type bond
$ ethtool -k bond0 | grep scatter
scatter-gather: off
tx-scatter-gather: off [requested on]
tx-scatter-gather-fraglist: off [requested on]
* create a vlan device
$ ip link add link bond0 name bond0.10 type vlan id 10
$ ethtool -k bond0.10 | grep scatter
scatter-gather: off
tx-scatter-gather: off
tx-scatter-gather-fraglist: off
* Add a slave device to bond0
$ ip link set dev eth0 master bond0
And now we can see that the bond0 device has got the scatter-gather
feature, but the bond0.10 hasn't got it.
[root@laptop linux-task-diag]# ethtool -k bond0 | grep scatter
scatter-gather: on
tx-scatter-gather: on
tx-scatter-gather-fraglist: on
[root@laptop linux-task-diag]# ethtool -k bond0.10 | grep scatter
scatter-gather: off
tx-scatter-gather: off
tx-scatter-gather-fraglist: off
With this patch the vlan device will get all new features from the
bonding device.
Here is a call trace how features which are set in this patch reach
dev->wanted_features.
register_netdevice
vlan_dev_init
...
dev->hw_features = NETIF_F_HW_CSUM | NETIF_F_SG |
NETIF_F_FRAGLIST | NETIF_F_GSO_SOFTWARE |
NETIF_F_HIGHDMA | NETIF_F_SCTP_CRC |
NETIF_F_ALL_FCOE;
dev->features |= dev->hw_features;
...
dev->wanted_features = dev->features & dev->hw_features;
__netdev_update_features(dev);
vlan_dev_fix_features
...
Cc: Alexey Kuznetsov <kuznet@virtuozzo.com>
Cc: Patrick McHardy <kaber@trash.net>
Cc: "David S. Miller" <davem@davemloft.net>
Signed-off-by: Andrei Vagin <avagin@openvz.org>
Signed-off-by: David S. Miller <davem@davemloft.net>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit c3883fe064 ]
This patch fixes an issue in drivers/hid/hid-input.c where values
outside of the logical range are not clamped when "null state" bit of
the input control is not set.
This was discussed on the lists [1] and this change stems from the fact
due to the ambiguity of the HID specification it might be appropriate to
follow Microsoft's own interpretation of the specification. As noted in
Microsoft's documentation [2] in the section titled "Required HID usages
for digitizers" it is noted that values reported outside the logical
range "will be considered as invalid data and the value will be changed
to the nearest boundary value (logical min/max)."
This patch fixes an issue where the (1292:4745) Innomedia INNEX
GENESIS/ATARI reports out of range values for its X and Y axis of the
DPad which, due to the null state bit being unset, are forwarded to
userspace as is. Now these values will get clamped to the logical range
before being forwarded to userspace. This device was also used to test
this patch.
This patch expands on commit 3f3752705d ("HID: reject input outside
logical range only if null state is set").
[1]: http://lkml.kernel.org/r/20170307131036.GA853@gaia.local
[2]: https://msdn.microsoft.com/en-us/library/windows/hardware/dn672278(v=vs.85).asp
Signed-off-by: Tomasz Kramkowski <tk@the-tk.com>
Acked-by: Benjamin Tissoires <benjamin.tissoires@redhat.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 0348aaa344 ]
dss_init_ports() is not handling return errors from dpi_init_port() and
sdi_init_port(). It is also always returning 0 currently which results in
part of error handling code in dss_bind() being unused.
Fix dss_init_ports() to handle return errors from dpi_init_port() and
sdi_init_port().
Signed-off-by: Arvind Yadav <arvind.yadav.cs@gmail.com>
Cc: tomi.valkeinen@ti.com
[b.zolnierkie: fail early on errors, minor fixups]
Signed-off-by: Bartlomiej Zolnierkiewicz <b.zolnierkie@samsung.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 5204bf1703 ]
When the MCA banks in __mcheck_cpu_init_generic() are polled for leftover
errors logged during boot or from the previous boot, its required to have
CPU features detected sufficiently so that the reading out and handling of
those early errors is done correctly.
If those features are not available, the decoding may miss some information
and get incomplete errors logged. For example, on SMCA systems the MCA_IPID
and MCA_SYND registers are not logged and MCA_ADDR is not masked
appropriately.
To cure that, do a subset of the basic feature detection early while the
rest happens in its usual place in __mcheck_cpu_init_vendor().
Signed-off-by: Yazen Ghannam <Yazen.Ghannam@amd.com>
Cc: Tony Luck <tony.luck@intel.com>
Cc: linux-edac <linux-edac@vger.kernel.org>
Cc: x86-ml <x86@kernel.org>
Link: http://lkml.kernel.org/r/1489599055-20756-1-git-send-email-Yazen.Ghannam@amd.com
[ Massage commit message and simplify. ]
Signed-off-by: Borislav Petkov <bp@suse.de>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 5080f39e8c ]
I recently reported on the netem list that iperf network benchmarks
show unexpected results when a bandwidth throttling rate has been
configured for netem. Specifically:
1) The measured link bandwidth *increases* when a higher delay is added
2) The measured link bandwidth appears higher than the specified limit
3) The measured link bandwidth for the same very slow settings varies significantly across
machines
The issue can be reproduced by using tc to configure netem with a
512kbit rate and various (none, 1us, 50ms, 100ms, 200ms) delays on a
veth pair between network namespaces, and then using iperf (or any
other network benchmarking tool) to test throughput. Complete detailed
instructions are in the original email chain here:
https://lists.linuxfoundation.org/pipermail/netem/2017-February/001672.html
There appear to be two underlying bugs causing these effects:
- The first issue causes long delays when the rate is slow and no
delay is configured (e.g., "rate 512kbit"). This is because SKBs are
not orphaned when no delay is configured, so orphaning does not
occur until *after* the rate-induced delay has been applied. For
this reason, adding a tiny delay (e.g., "rate 512kbit delay 1us")
dramatically increases the measured bandwidth.
- The second issue is that rate-induced delays are not correctly
applied, allowing SKB delays to occur in parallel. The indended
approach is to compute the delay for an SKB and to add this delay to
the end of the current queue. However, the code does not detect
existing SKBs in the queue due to improperly testing sch->q.qlen,
which is nonzero even when packets exist only in the
rbtree. Consequently, new SKBs do not wait for the current queue to
empty. When packet delays vary significantly (e.g., if packet sizes
are different), then this also causes unintended reordering.
I modified the code to expect a delay (and orphan the SKB) when a rate
is configured. I also added some defensive tests that correctly find
the latest scheduled delivery time, even if it is (unexpectedly) for a
packet in sch->q. I have tested these changes on the latest kernel
(4.11.0-rc1+) and the iperf / ping test results are as expected.
Signed-off-by: Nik Unger <njunger@uwaterloo.ca>
Signed-off-by: Stephen Hemminger <stephen@networkplumber.org>
Signed-off-by: David S. Miller <davem@davemloft.net>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit bdd3c25423 ]
Currently bcm2835_defconfig has CMA disabled which makes the
HDMI output on a Raspberry Pi 1 stop working during boot:
fb: switching to vc4drmfb from simple
Console: switching to colour dummy device 80x30
[drm] Initialized vc4 0.0.0 20140616 for soc:gpu on minor 0
[drm] Supports vblank timestamp caching Rev 2 (21.10.2013).
[drm] Driver supports precise vblank timestamp query.
vc4-drm soc:gpu: failed to allocate buffer with size 9216000
vc4-drm soc:gpu: Failed to set initial hw configuration.
So enable CMA and DMA_CMA in bcm2835_defconfig.
Signed-off-by: Stefan Wahren <stefan.wahren@i2se.com>
Fixes: 4400d9ac05 ("ARM: bcm2835: Enable the VC4 graphics driver in the defconfig")
Reviewed-by: Eric Anholt <eric@anholt.net>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit c4ba329cab ]
There is a small window during which the an URB may
remain active after disconnect has returned. If in that case
already freed memory may be accessed and executed.
The fix is to poison the URB befotre the work is flushed.
Signed-off-by: Oliver Neukum <oneukum@suse.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit a28f6f27a8 ]
Fetch target operating channel during potential radar detection when
the interface is just brought up, but no channel is assigned from
userspace. In this scenario rx_channel may not be having a valid pointer
hence fetch the target operating channel to avoid warnings as below
which can be triggered by the commands with DFS testing over longer run
comamnds:
iw wlan1 set type mesh
ifconfig wlan1 up (valid tgt_oper_chan only)
iw wlan1 cac trigger freq 5260 HT20 (valid rx_channel, tgt_oper_chan)
iw wlan1 cac trigger freq 5280 HT20
iw wlan1 cac trigger freq 5300 HT20
Once the CAC expires, current channel context will be removed and
we are only left with the fallback option of using 'target operating
channel'
Firmware and driver log:
ath: phy1: DFS: radar found on freq=5300: id=1, pri=1125, count=5,
count_false=4
ath: phy1: DFS: radar found on freq=5260: id=5, pri=3151, count=6,
count_false=11
ath: phy1: DFS: radar found on freq=5280: id=1, pri=1351, count=6,
count_false=4
ath: phy1: DFS: radar found on freq=5300: id=1, pri=1125, count=5,
count_false=4
ath10k_pci 0001:01:00.0: failed to derive channel for radar pulse,
treating as radar
ath10k_pci 0001:01:00.0: failed to derive channel for radar pulse,
treating as radar
Call trace:
WARNING: CPU: 1 PID: 2145 at
backports-20161201-3.14.77-9ab3068/net/wireless/chan.c:265
cfg80211_set_dfs_state+0x3c/0x88 [cfg80211]()
Workqueue: phy1 ieee80211_dfs_radar_detected_work
[mac80211]
[<c0320770>] (warn_slowpath_null) from [<bf79b90c>]
(cfg80211_set_dfs_state+0x3c/0x88 [cfg80211])
[<bf79b90c>] (cfg80211_set_dfs_state [cfg80211]) from
[<bf79697c>] (cfg80211_radar_event+0xc4/0x140 [cfg80211])
[<bf79697c>] (cfg80211_radar_event [cfg80211]) from
[<bf83c058>] (ieee80211_dfs_radar_detected_work+0xa8/0xb4 [mac80211])
[<bf83c058>] (ieee80211_dfs_radar_detected_work
[mac80211]) from [<c0339518>] (process_one_work+0x298/0x4a4)
Signed-off-by: Mohammed Shafi Shajakhan <mohammed@qti.qualcomm.com>
Signed-off-by: Kalle Valo <kvalo@qca.qualcomm.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit ca07baab0b ]
If DFS is not enabled in hostapd (ieee80211h=0) DFS channels shall
not be available for use even though the hardware may have the capability
to support DFS. With this configuration (DFS disabled in hostapd) trying to
bring up ath10k device in DFS channel for AP mode fails and trying to
simulate DFS in ath10k debugfs results in a warning in cfg80211 complaining
invalid channel and this should be avoided in the driver itself rather than
false propogating RADAR detection to mac80211/cfg80211. Fix this by
checking for the first vif 'is_started' state(should work for client mode
as well) as all the vifs shall be configured for the same channel
sys/kernel/debug/ieee80211/phy1/ath10k# echo 1 > dfs_simulate_radar
WARNING: at net/wireless/chan.c:265 cfg80211_radar_event+0x24/0x60
Workqueue: phy0 ieee80211_dfs_radar_detected_work [mac80211]
[<c022f2d4>] (warn_slowpath_null) from
[<bf72dab8>] (cfg80211_radar_event+0x24/0x60 [cfg80211])
[<bf72dab8>] (cfg80211_radar_event [cfg80211]) from
[<bf7813e0>] (ieee80211_dfs_radar_detected_work+0x94/0xa0 [mac80211])
[<bf7813e0>] (ieee80211_dfs_radar_detected_work [mac80211]) from
[<c0242320>] (process_one_work+0x20c/0x32c)
WARNING: at net/wireless/nl80211.c:2488 nl80211_get_mpath+0x13c/0x4cc
Workqueue: phy0 ieee80211_dfs_radar_detected_work [mac80211]
[<c022f2d4>] (warn_slowpath_null) from
[<bf72dab8>] (cfg80211_radar_event+0x24/0x60 [cfg80211])
[<bf72dab8>] (cfg80211_radar_event [cfg80211]) from
[<bf7813e0>] (ieee80211_dfs_radar_detected_work+0x94/0xa0 [mac80211])
[<bf7813e0>] (ieee80211_dfs_radar_detected_work [mac80211]) from
[<c0242320>] (process_one_work+0x20c/0x32c)
Signed-off-by: Mohammed Shafi Shajakhan <mohammed@qti.qualcomm.com>
Signed-off-by: Kalle Valo <kvalo@qca.qualcomm.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 608b205069 ]
On vblank instant-off systems, we can get into a situation where the cost
of enabling and disabling the vblank IRQ around a drmWaitVblank query
dominates. And with the advent of even deeper hardware sleep state,
touching registers becomes ever more expensive. However, we know that if
the user wants the current vblank counter, they are also very likely to
immediately queue a vblank wait and so we can keep the interrupt around
and only turn it off if we have no further vblank requests queued within
the interrupt interval.
After vblank event delivery, this patch adds a shadow of one vblank where
the interrupt is kept alive for the user to query and queue another vblank
event. Similarly, if the user is using blocking drmWaitVblanks, the
interrupt will be disabled on the IRQ following the wait completion.
However, if the user is simply querying the current vblank counter and
timestamp, the interrupt will be disabled after every IRQ and the user
will enabled it again on the first query following the IRQ.
v2: Mario Kleiner -
After testing this, one more thing that would make sense is to move
the disable block at the end of drm_handle_vblank() instead of at the
top.
Turns out that if high precision timestaming is disabled or doesn't
work for some reason (as can be simulated by echo 0 >
/sys/module/drm/parameters/timestamp_precision_usec), then with your
delayed disable code at its current place, the vblank counter won't
increment anymore at all for instant queries, ie. with your other
"instant query" patches. Clients which repeatedly query the counter
and wait for it to progress will simply hang, spinning in an endless
query loop. There's that comment in vblank_disable_and_save:
"* Skip this step if there isn't any high precision timestamp
* available. In that case we can't account for this and just
* hope for the best.
*/
With the disable happening after leading edge of vblank (== hw counter
increment already happened) but before the vblank counter/timestamp
handling in drm_handle_vblank, that step is needed to keep the counter
progressing, so skipping it is bad.
Now without high precision timestamping support, a kms driver must not
set dev->vblank_disable_immediate = true, as this would cause problems
for clients, so this shouldn't matter, but it would be good to still
make this robust against a future kms driver which might have
unreliable high precision timestamping, e.g., high precision
timestamping that intermittently doesn't work.
v3: Patch before coffee needs extra coffee.
Testcase: igt/kms_vblank
Signed-off-by: Chris Wilson <chris@chris-wilson.co.uk>
Cc: Ville Syrjälä <ville.syrjala@linux.intel.com>
Cc: Daniel Vetter <daniel@ffwll.ch>
Cc: Michel Dänzer <michel@daenzer.net>
Cc: Laurent Pinchart <laurent.pinchart@ideasonboard.com>
Cc: Dave Airlie <airlied@redhat.com>,
Cc: Mario Kleiner <mario.kleiner.de@gmail.com>
Reviewed-by: Ville Syrjälä <ville.syrjala@linux.intel.com>
Signed-off-by: Daniel Vetter <daniel.vetter@ffwll.ch>
Link: http://patchwork.freedesktop.org/patch/msgid/20170315204027.20160-1-chris@chris-wilson.co.uk
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 3c51b9c7f1 ]
Some Host Controller hardware blocks, like the OHCI, EHCI and SDIO
controllers, have hardware blocks that are not capable of doing 64 bit
DMA. These host controllers fail on boards with >3GB of memory because
the memory above 3GB is located physically >= 0x100000000 and can only
be accessed using 64 DMA. The way Linux is currently configured for
BRCMSTB systems, the memory given to drivers for DMA through functions
like dma_alloc_coherent() comes from CMA memory and CMA memory is taken
from the top of physical memory. When these drivers get a DMA buffer
with an address >=0x100000000, they end up dropping the upper 32 bit of
the address causing the hardware to DMA to incorrect memory, typically
BMEM (custom memory carveout). This issue was discovered on a
BCM97449SSV_DDR4 system with 4GB or memory.
The fix is to enable CONFIG_ZONE_DMA. On ARM systems this makes sure
that all DMA memory is located within the first 32 bits of address
space.
Signed-off-by: Al Cooper <alcooperx@gmail.com>
Signed-off-by: Florian Fainelli <f.fainelli@gmail.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 88b897a30c ]
This patch significantly improves the execution time of
perf_event__synthesize_mmap_events() when running perf record on systems
where processes have lots of threads.
It just happens that cat /proc/pid/maps support uses a O(N^2) algorithm to
generate each map line in the maps file. If you have 1000 threads, then you
have necessarily 1000 stacks. For each vma, you need to check if it
corresponds to a thread's stack. With a large number of threads, this can take
a very long time. I have seen latencies >> 10mn.
As of today, perf does not use the fact that a mapping is a stack, therefore we
can work around the issue by using /proc/pid/tasks/pid/maps. This entry does
not try to map a vma to stack and is thus much faster with no loss of
functonality.
The proc-map-timeout logic is kept in case users still want some upper limit.
In V2, we fix the file path from /proc/pid/tasks/pid/maps to actual
/proc/pid/task/pid/maps, tasks -> task. Thanks Arnaldo for catching this.
Committer note:
This problem seems to have been elliminated in the kernel since commit :
b18cb64ead ("fs/proc: Stop trying to report thread stacks").
Signed-off-by: Stephane Eranian <eranian@google.com>
Acked-by: Jiri Olsa <jolsa@redhat.com>
Cc: Andy Lutomirski <luto@kernel.org>
Cc: Namhyung Kim <namhyung@kernel.org>
Cc: Peter Zijlstra <peterz@infradead.org>
Link: http://lkml.kernel.org/r/20170315135059.GC2177@redhat.com
Link: http://lkml.kernel.org/r/1489598233-25586-1-git-send-email-eranian@google.com
Signed-off-by: Arnaldo Carvalho de Melo <acme@redhat.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit c271dd6c39 ]
Currently ethtool -e will error out with a X722 interface
as its EEPROM has a scope limit at offset 0x5B9FFF.
This patch fixes the issue by setting the EEPROM length to
the scope limit to avoid NVM read failure beyond that.
Change-ID: I0b7d4dd6c7f2a57cace438af5dffa0f44c229372
Signed-off-by: Lihong Yang <lihong.yang@intel.com>
Tested-by: Andrew Bowers <andrewx.bowers@intel.com>
Signed-off-by: Jeff Kirsher <jeffrey.t.kirsher@intel.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 6f051e4a68 ]
[resend due to me forgetting to cc: linux-api the first time around I
posted these back on Feb 23]
From: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When userspace tries to use these defines, it complains that it needs to
be an unsigned 1 that is shifted, so libc implementations have to create
their own version. Fix this by defining it properly so that libcs can
just use the kernel uapi header.
Reported-by: Elliott Hughes <enh@google.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 3e6ef9c809 ]
mmap(MAP_32BIT) is broken due to the dependency on the TIF_ADDR32 thread
flag.
For 64bit applications MAP_32BIT will force legacy bottom-up allocations and
the 1GB address space restriction even if the application issued a compat
syscall, which should not be subject of these restrictions.
For 32bit applications, which issue 64bit syscalls the newly introduced
mmap base separation into 64-bit and compat bases changed the behaviour
because now a 64-bit mapping is returned, but due to the TIF_ADDR32
dependency MAP_32BIT is ignored. Before the separation a 32-bit mapping was
returned, so the MAP_32BIT handling was irrelevant.
Replace the check for TIF_ADDR32 with a check for the compat syscall. That
solves both the 64-bit issuing a compat syscall and the 32-bit issuing a
64-bit syscall problems.
[ tglx: Massaged changelog ]
Signed-off-by: Dmitry Safonov <dsafonov@virtuozzo.com>
Cc: 0x7f454c46@gmail.com
Cc: linux-mm@kvack.org
Cc: Andy Lutomirski <luto@kernel.org>
Cc: Cyrill Gorcunov <gorcunov@openvz.org>
Cc: Borislav Petkov <bp@suse.de>
Cc: "Kirill A. Shutemov" <kirill.shutemov@linux.intel.com>
Link: http://lkml.kernel.org/r/20170306141721.9188-5-dsafonov@virtuozzo.com
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit e2f586bd83 ]
KMSAN (KernelMemorySanitizer, a new error detection tool) reports use of
uninitialized memory in selinux_socket_bind():
==================================================================
BUG: KMSAN: use of unitialized memory
inter: 0
CPU: 3 PID: 1074 Comm: packet2 Tainted: G B 4.8.0-rc6+ #1916
Hardware name: QEMU Standard PC (i440FX + PIIX, 1996), BIOS Bochs 01/01/2011
0000000000000000 ffff8800882ffb08 ffffffff825759c8 ffff8800882ffa48
ffffffff818bf551 ffffffff85bab870 0000000000000092 ffffffff85bab550
0000000000000000 0000000000000092 00000000bb0009bb 0000000000000002
Call Trace:
[< inline >] __dump_stack lib/dump_stack.c:15
[<ffffffff825759c8>] dump_stack+0x238/0x290 lib/dump_stack.c:51
[<ffffffff818bdee6>] kmsan_report+0x276/0x2e0 mm/kmsan/kmsan.c:1008
[<ffffffff818bf0fb>] __msan_warning+0x5b/0xb0 mm/kmsan/kmsan_instr.c:424
[<ffffffff822dae71>] selinux_socket_bind+0xf41/0x1080 security/selinux/hooks.c:4288
[<ffffffff8229357c>] security_socket_bind+0x1ec/0x240 security/security.c:1240
[<ffffffff84265d98>] SYSC_bind+0x358/0x5f0 net/socket.c:1366
[<ffffffff84265a22>] SyS_bind+0x82/0xa0 net/socket.c:1356
[<ffffffff81005678>] do_syscall_64+0x58/0x70 arch/x86/entry/common.c:292
[<ffffffff8518217c>] entry_SYSCALL64_slow_path+0x25/0x25 arch/x86/entry/entry_64.o:?
chained origin: 00000000ba6009bb
[<ffffffff810bb7a7>] save_stack_trace+0x27/0x50 arch/x86/kernel/stacktrace.c:67
[< inline >] kmsan_save_stack_with_flags mm/kmsan/kmsan.c:322
[< inline >] kmsan_save_stack mm/kmsan/kmsan.c:337
[<ffffffff818bd2b8>] kmsan_internal_chain_origin+0x118/0x1e0 mm/kmsan/kmsan.c:530
[<ffffffff818bf033>] __msan_set_alloca_origin4+0xc3/0x130 mm/kmsan/kmsan_instr.c:380
[<ffffffff84265b69>] SYSC_bind+0x129/0x5f0 net/socket.c:1356
[<ffffffff84265a22>] SyS_bind+0x82/0xa0 net/socket.c:1356
[<ffffffff81005678>] do_syscall_64+0x58/0x70 arch/x86/entry/common.c:292
[<ffffffff8518217c>] return_from_SYSCALL_64+0x0/0x6a arch/x86/entry/entry_64.o:?
origin description: ----address@SYSC_bind (origin=00000000b8c00900)
==================================================================
(the line numbers are relative to 4.8-rc6, but the bug persists upstream)
, when I run the following program as root:
=======================================================
#include <string.h>
#include <sys/socket.h>
#include <netinet/in.h>
int main(int argc, char *argv[]) {
struct sockaddr addr;
int size = 0;
if (argc > 1) {
size = atoi(argv[1]);
}
memset(&addr, 0, sizeof(addr));
int fd = socket(PF_INET6, SOCK_DGRAM, IPPROTO_IP);
bind(fd, &addr, size);
return 0;
}
=======================================================
(for different values of |size| other error reports are printed).
This happens because bind() unconditionally copies |size| bytes of
|addr| to the kernel, leaving the rest uninitialized. Then
security_socket_bind() reads the IP address bytes, including the
uninitialized ones, to determine the port, or e.g. pass them further to
sel_netnode_find(), which uses them to calculate a hash.
Signed-off-by: Alexander Potapenko <glider@google.com>
Acked-by: Eric Dumazet <edumazet@google.com>
[PM: fixed some whitespace damage]
Signed-off-by: Paul Moore <paul@paul-moore.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit fda78d7a0e ]
The pci_bus_type .shutdown method, pci_device_shutdown(), is called from
device_shutdown() in the kernel restart and shutdown paths.
Previously, pci_device_shutdown() called pci_msi_shutdown() and
pci_msix_shutdown(). This disables MSI and MSI-X, which causes the device
to fall back to raising interrupts via INTx. But the driver is still bound
to the device, it doesn't know about this change, and it likely doesn't
have an INTx handler, so these INTx interrupts cause "nobody cared"
warnings like this:
irq 16: nobody cared (try booting with the "irqpoll" option)
CPU: 0 PID: 0 Comm: swapper/0 Not tainted 4.8.2-1.el7_UNSUPPORTED.x86_64 #1
Hardware name: Hewlett-Packard HP Z820 Workstation/158B, BIOS J63 v03.90 06/
...
The MSI disabling code was added by d52877c7b1 ("pci/irq: let
pci_device_shutdown to call pci_msi_shutdown v2") because a driver left MSI
enabled and kdump failed because the kexeced kernel wasn't prepared to
receive the MSI interrupts.
Subsequent commits 1851617cd2 ("PCI/MSI: Disable MSI at enumeration even
if kernel doesn't support MSI") and e80e7edc55 ("PCI/MSI: Initialize MSI
capability for all architectures") changed the kexeced kernel to disable
all MSIs itself so it no longer depends on the crashed kernel to clean up
after itself.
Stop disabling MSI/MSI-X in pci_device_shutdown(). This resolves the
"nobody cared" unhandled IRQ issue above. It also allows PCI serial
devices, which may rely on the MSI interrupts, to continue outputting
messages during reboot/shutdown.
[bhelgaas: changelog, drop pci_msi_shutdown() and pci_msix_shutdown() calls
altogether]
Fixes: https://bugzilla.kernel.org/show_bug.cgi?id=187351
Signed-off-by: Prarit Bhargava <prarit@redhat.com>
Signed-off-by: Bjorn Helgaas <bhelgaas@google.com>
CC: Alex Williamson <alex.williamson@redhat.com>
CC: David Arcari <darcari@redhat.com>
CC: Myron Stowe <mstowe@redhat.com>
CC: Lukas Wunner <lukas@wunner.de>
CC: Keith Busch <keith.busch@intel.com>
CC: Mika Westerberg <mika.westerberg@linux.intel.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 4c7f16d14a ]
The TCON driver calls sun4i_tcon_init_regmap and sun4i_tcon_init_clocks
in its bind function. The former creates a regmap and writes to several
register to clear its configuration to a known default. The latter
initializes various clocks. This includes enabling the bus clock for
register access and creating the dotclock.
In order for the first step's writes to work, the bus clock must be
enabled which is done in the second step. but the dotclock's ops use
the regmap created in the first step.
Rearrange the function calls such that the clocks are initialized before
the regmap, and split out the dot clock creation to after the regmap is
initialized.
Fixes: 9026e0d122 ("drm: Add Allwinner A10 Display Engine support")
Signed-off-by: Chen-Yu Tsai <wens@csie.org>
Signed-off-by: Maxime Ripard <maxime.ripard@free-electrons.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit c73f8c0033 ]
Doing a channel switch via hostapd_cli seems to update
the new channel context for each VAP's appropriately as below
in 'ath10k_mac_update_vif_chan', hence we can safely suppress the
warning that shows up during this operation and dump the warning only
if no vaps are available for channel switch
hostapd_cli -i wlan0 chan_switch 5 5200
OK
ath10k_pci : mac chanctx switch n_vifs 3 mode 1
ath10k_pci : mac chanctx switch vdev_id 2 freq 5180->5200 width 0->0
ath10k_pci : mac chanctx switch vdev_id 1 freq 5180->5200 width 0->0
ath10k_pci : mac chanctx switch vdev_id 0 freq 5180->5200 width 0->0
Call Trace:
WARNING: backports-20161201-3.14.77-9ab3068/drivers/net/wireless/ath/ath10k/mac.c:7126
[<c022f2d4>] (warn_slowpath_null) from [<bf7f150c>]
(ath10k_reconfig_complete+0xe4/0x25c [ath10k_core])
[<bf7f150c>] (ath10k_reconfig_complete [ath10k_core])
[<bf7f35f0>] (ath10k_mac_vif_ap_csa_work+0x214/0x370 [ath10k_core])
[<bf7f38b8>] (ath10k_mac_op_change_chanctx+0x108/0x128 [ath10k_core])
[<bf782ac0>] (ieee80211_recalc_chanctx_min_def+0x30c/0x430 [mac80211])
[<bf7830a4>] (ieee80211_recalc_smps_chanctx+0x2ec/0x840 [mac80211])
[<bf7843e8>] (ieee80211_vif_use_reserved_context+0x7c/0xf8 [mac80211])
[<bf7843e8>] (ieee80211_vif_use_reserved_context [mac80211])
[<bf76e5d4>] (ieee80211_csa_finalize_work+0x5c/0x88 [mac80211])
Fixes: d7bf4b4aba ("ath10k: fix ar->rx_channel updating logic")
Signed-off-by: Mohammed Shafi Shajakhan <mohammed@qti.qualcomm.com>
Signed-off-by: Kalle Valo <kvalo@qca.qualcomm.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 7544860733 ]
The way drm_of_find_possible_crtcs works is it tries to match the
remote-endpoint of the given node's various endpoints to all the
crtc's .port field. Thus we need to set drm_crtc.port to the output
port node of the underlying TCON.
Signed-off-by: Chen-Yu Tsai <wens@csie.org>
Signed-off-by: Maxime Ripard <maxime.ripard@free-electrons.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 9d56defb44 ]
The master bind function calls numerous drm functions which initialize
underlying structures. It also tries to bind the various components
of the display pipeline, some of which may add additional drm objects.
This patch adds proper cleanup functions in the error path of the
master bind function.
This requires the patch "drm/sun4i: Move drm_mode_config_cleanup call
to main driver", which splits out drm_mode_config_cleanup from
sun4i_framebuffer_free so we can call it separately.
Signed-off-by: Chen-Yu Tsai <wens@csie.org>
Signed-off-by: Maxime Ripard <maxime.ripard@free-electrons.com>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 57a4fd420c ]
The Cortex-A57 cache controller is an integrated controller, and thus
the device node representing it should not have a unit-addresses or reg
property.
Fixes: 1561f20760 ("arm64: dts: r8a7796: Add Renesas R8A7796 SoC support")
Signed-off-by: Geert Uytterhoeven <geert+renesas@glider.be>
Signed-off-by: Simon Horman <horms+renesas@verge.net.au>
Signed-off-by: Sasha Levin <alexander.levin@microsoft.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>