commit d1ee66c5d3 upstream.
Fix two bugs with the Intel HDA Realtek ALC233 sound codec
present in Intel NUC NUC8i7BEH and probably a few other similar
NUC models.
These codecs advertise a 4-level microphone input boost amplifier on
pin 0x19, but the highest two boost settings do not work correctly,
and produce only low analog noise that does not seem to contain any
discernible signal. There is an existing fixup for this exact problem
but for a different PCI subsystem ID, so we re-use that logic.
Changing the boost level also triggers a DC spike in the input signal
that bleeds off over about a second and overwhelms any input during
that time. Thankfully, the existing fixup has the side effect of
making the boost control show up in userspace as a mute/unmute switch,
and this keeps (e.g.) PulseAudio from fiddling with it during normal
input volume adjustments.
Finally, the NUC hardware has built-in inverted stereo mics. This
patch also enables the usual fixup for this so the two channels cancel
noise instead of the actual signal.
[ Re-ordered the quirk entry point by tiwai ]
Signed-off-by: Phil Calvin <phil@philcalvin.com>
Cc: <stable@vger.kernel.org>
Link: https://lore.kernel.org/r/80dc5663-7734-e7e5-25ef-15b5df24511a@philcalvin.com
Signed-off-by: Takashi Iwai <tiwai@suse.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 4fb44dd2c1 upstream.
In snd_sb_qsound_build, snd_ctl_add(..,p->qsound_switch...) and
snd_ctl_add(..,p->qsound_space..) are called. But the second
arguments of snd_ctl_add() could be freed via snd_ctl_add_replace()
->snd_ctl_free_one(). After the error code is returned,
snd_sb_qsound_destroy(p) is called in __error branch.
But in snd_sb_qsound_destroy(), the freed p->qsound_switch and
p->qsound_space are still used by snd_ctl_remove().
My patch set p->qsound_switch and p->qsound_space to NULL if
snd_ctl_add() failed to avoid the uaf bugs. But these codes need
to further be improved with the code style.
Signed-off-by: Lv Yunlong <lyl2019@mail.ustc.edu.cn>
Cc: <stable@vger.kernel.org>
Link: https://lore.kernel.org/r/20210426145541.8070-1-lyl2019@mail.ustc.edu.cn
Signed-off-by: Takashi Iwai <tiwai@suse.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 1c98f57440 upstream.
Our code analyzer reported a uaf.
In snd_emu8000_create_mixer, the callee snd_ctl_add(..,emu->controls[i])
calls snd_ctl_add_replace(.., kcontrol,..). Inside snd_ctl_add_replace(),
if error happens, kcontrol will be freed by snd_ctl_free_one(kcontrol).
Then emu->controls[i] points to a freed memory, and the execution comes
to __error branch of snd_emu8000_create_mixer. The freed emu->controls[i]
is used in snd_ctl_remove(card, emu->controls[i]).
My patch set emu->controls[i] to NULL if snd_ctl_add() failed to avoid
the uaf.
Signed-off-by: Lv Yunlong <lyl2019@mail.ustc.edu.cn>
Cc: <stable@vger.kernel.org>
Link: https://lore.kernel.org/r/20210426131129.4796-1-lyl2019@mail.ustc.edu.cn
Signed-off-by: Takashi Iwai <tiwai@suse.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit d0a43c12ee ]
Fix invalid usage of a list_for_each_entry in cpcap_battery_irq_thread().
Empty list or fully traversed list points to list head, which is not
NULL (and before the first element containing real data).
Signed-off-by: Guangqing Zhu <zhuguangqing83@gmail.com>
Reviewed-by: Tony Lindgren <tony@atomide.com>
Reviewed-by: Carl Philipp Klemm <philipp@uvos.xyz>
Tested-by: Carl Philipp Klemm <philipp@uvos.xyz>
Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 9d10a13d1e ]
psi_group_cpu->tasks, represented by the unsigned int, stores the
number of tasks that could be stalled on a psi resource(io/mem/cpu).
Decrementing these counters at zero leads to wrapping which further
leads to the psi_group_cpu->state_mask is being set with the
respective pressure state. This could result into the unnecessary time
sampling for the pressure state thus cause the spurious psi events.
This can further lead to wrong actions being taken at the user land
based on these psi events.
Though psi_bug is set under these conditions but that just for debug
purpose. Fix it by decrementing the ->tasks count only when it is
non-zero.
Signed-off-by: Charan Teja Reddy <charante@codeaurora.org>
Signed-off-by: Peter Zijlstra (Intel) <peterz@infradead.org>
Acked-by: Johannes Weiner <hannes@cmpxchg.org>
Link: https://lkml.kernel.org/r/1618585336-37219-1-git-send-email-charante@codeaurora.org
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 2809606768 ]
A review of the code showed, that this function which is exposed
within the whole kernel should do a parameter check for the
amount of bytes requested. If this requested bytes is too high
an unsigned int overflow could happen causing this function to
try to memcpy a really big memory chunk.
This is not a security issue as there are only two invocations
of this function from arch/s390/include/asm/archrandom.h and both
are not exposed to userland.
Reported-by: Sven Schnelle <svens@linux.ibm.com>
Signed-off-by: Harald Freudenberger <freude@linux.ibm.com>
Signed-off-by: Heiko Carstens <hca@linux.ibm.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 12b0653310 ]
When unloading the rnbd-clt module, it does not free a memory
including the filename of the symbolic link to /sys/block/rnbdX.
It is found by kmemleak as below.
unreferenced object 0xffff9f1a83d3c740 (size 16):
comm "bash", pid 736, jiffies 4295179665 (age 9841.310s)
hex dump (first 16 bytes):
21 64 65 76 21 6e 75 6c 6c 62 30 40 62 6c 61 00 !dev!nullb0@bla.
backtrace:
[<0000000039f0c55e>] 0xffffffffc0456c24
[<000000001aab9513>] kernfs_fop_write+0xcf/0x1c0
[<00000000db5aa4b3>] vfs_write+0xdb/0x1d0
[<000000007a2e2207>] ksys_write+0x65/0xe0
[<00000000055e280a>] do_syscall_64+0x50/0x1b0
[<00000000c2b51831>] entry_SYSCALL_64_after_hwframe+0x49/0xbe
Signed-off-by: Gioh Kim <gi-oh.kim@ionos.com>
Signed-off-by: Jack Wang <jinpu.wang@ionos.com>
Link: https://lore.kernel.org/r/20210419073722.15351-13-gi-oh.kim@ionos.com
Signed-off-by: Jens Axboe <axboe@kernel.dk>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 0c2de3f054 ]
The current sched_slice() seems to have issues; there's two possible
things that could be improved:
- the 'nr_running' used for __sched_period() is daft when cgroups are
considered. Using the RQ wide h_nr_running seems like a much more
consistent number.
- (esp) cgroups can slice it real fine, which makes for easy
over-scheduling, ensure min_gran is what the name says.
Signed-off-by: Peter Zijlstra (Intel) <peterz@infradead.org>
Tested-by: Valentin Schneider <valentin.schneider@arm.com>
Link: https://lkml.kernel.org/r/20210412102001.611897312@infradead.org
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit ef54c1a476 ]
Make perf_event_exit_event() more robust, such that we can use it from
other contexts. Specifically the up and coming remove_on_exec.
For this to work we need to address a few issues. Remove_on_exec will
not destroy the entire context, so we cannot rely on TASK_TOMBSTONE to
disable event_function_call() and we thus have to use
perf_remove_from_context().
When using perf_remove_from_context(), there's two races to consider.
The first is against close(), where we can have concurrent tear-down
of the event. The second is against child_list iteration, which should
not find a half baked event.
To address this, teach perf_remove_from_context() to special case
!ctx->is_active and about DETACH_CHILD.
[ elver@google.com: fix racing parent/child exit in sync_child_event(). ]
Signed-off-by: Marco Elver <elver@google.com>
Signed-off-by: Peter Zijlstra (Intel) <peterz@infradead.org>
Link: https://lkml.kernel.org/r/20210408103605.1676875-2-elver@google.com
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 90d6697810 ]
Since the 'mfs' member has been declared as 'u32' in include/scsi/libfc.h,
use the %u format specifier instead of %hu. This patch fixes the following
clang compiler warning:
warning: format specifies type
'unsigned short' but the argument has type 'u32' (aka 'unsigned int')
[-Wformat]
"lport->mfs:%hu\n", mfs, lport->mfs);
~~~ ^~~~~~~~~~
%u
Link: https://lore.kernel.org/r/20210415220826.29438-8-bvanassche@acm.org
Cc: Hannes Reinecke <hare@suse.de>
Signed-off-by: Bart Van Assche <bvanassche@acm.org>
Signed-off-by: Martin K. Petersen <martin.petersen@oracle.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit fe6df2b480 ]
pm_runtime_get_sync() will increase the rumtime PM counter
even it returns an error. Thus a pairing decrement is needed
to prevent refcount leak. Fix this by replacing this API with
pm_runtime_resume_and_get(), which will not change the runtime
PM counter on error.
Signed-off-by: Dinghao Liu <dinghao.liu@zju.edu.cn>
Acked-by: Charles Keepax <ckeepax@opensource.cirrus.com>
Signed-off-by: Lee Jones <lee.jones@linaro.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 586478bfc9 ]
By default the PMIC DA9063 2-wire interface is SMBus compliant. This
means the PMIC will automatically reset the interface when the clock
signal ceases for more than the SMBus timeout of 35 ms.
If the I2C driver / device is not capable of creating atomic I2C
transactions, a context change can cause a ceasing of the clock signal.
This can happen if for example a real-time thread is scheduled. Then
the DA9063 in SMBus mode will reset the 2-wire interface. Subsequently
a write message could end up in the wrong register. This could cause
unpredictable system behavior.
The DA9063 PMIC also supports an I2C compliant mode for the 2-wire
interface. This mode does not reset the interface when the clock
signal ceases. Thus the problem depicted above does not occur.
This patch tests for the bus functionality "I2C_FUNC_I2C". It can
reasonably be assumed that the bus cannot obey SMBus timings if
this functionality is set. SMBus commands most probably are emulated
in this case which is prone to the latency issue described above.
This patch enables the I2C bus mode if I2C_FUNC_I2C is set or
otherwise keeps the default SMBus mode.
Signed-off-by: Hubert Streidl <hubert.streidl@de.bosch.com>
Signed-off-by: Mark Jonas <mark.jonas@de.bosch.com>
Reviewed-by: Wolfram Sang <wsa+renesas@sang-engineering.com>
Signed-off-by: Lee Jones <lee.jones@linaro.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit d9b326b2c3 ]
This patch fixes the max register address of MAX 10 BMC. The range
0x20000000 ~ 0x200000fc are for control registers of the QSPI flash
controller, which are not accessible to host.
Signed-off-by: Xu Yilun <yilun.xu@intel.com>
Reviewed-by: Tom Rix <trix@redhat.com>
Signed-off-by: Lee Jones <lee.jones@linaro.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 304ee43238 ]
In SLI-4, when performing a mailbox command with MBX_POLL, the driver uses
the BMBX register to send the command rather than the MQ. A flag is set
indicating the BMBX register is active and saves the mailbox job struct
(mboxq) in the mbox_active element of the adapter. The routine then waits
for completion or timeout. The mailbox job struct is not freed by the
routine. In cases of timeout, the adapter will be reset. The
lpfc_sli_mbox_sys_flush() routine will clean up the mbox in preparation for
the reset. It clears the BMBX active flag and marks the job structure as
MBX_NOT_FINISHED. But, it never frees the mboxq job structure. Expectation
in both normal completion and timeout cases is that the issuer of the mbx
command will free the structure. Unfortunately, not all calling paths are
freeing the memory in cases of error.
All calling paths were looked at and updated, if missing, to free the mboxq
memory regardless of completion status.
Link: https://lore.kernel.org/r/20210412013127.2387-7-jsmart2021@gmail.com
Co-developed-by: Justin Tee <justin.tee@broadcom.com>
Signed-off-by: Justin Tee <justin.tee@broadcom.com>
Signed-off-by: James Smart <jsmart2021@gmail.com>
Signed-off-by: Martin K. Petersen <martin.petersen@oracle.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit fffd18ec65 ]
Fix a crash caused by a double put on the node when the driver completed an
ACC for an unsolicted abort on the same node. The second put was executed
by lpfc_nlp_not_used() and is wrong because the completion routine executes
the nlp_put when the iocbq was released. Additionally, the driver is
issuing a LOGO then immediately calls lpfc_nlp_set_state to put the node
into NPR. This call does nothing.
Remove the lpfc_nlp_not_used call and additional set_state in the
completion routine. Remove the lpfc_nlp_set_state post issue_logo. Isn't
necessary.
Link: https://lore.kernel.org/r/20210412013127.2387-3-jsmart2021@gmail.com
Co-developed-by: Justin Tee <justin.tee@broadcom.com>
Signed-off-by: Justin Tee <justin.tee@broadcom.com>
Signed-off-by: James Smart <jsmart2021@gmail.com>
Signed-off-by: Martin K. Petersen <martin.petersen@oracle.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 68eb3ae3c6 ]
When encoder validation of a display mode fails, retry with less bandwidth
heavy YCbCr420 color mode, if available. This enables some HDMI 1.4 setups
to support 4k60Hz output, which previously failed silently.
On some setups, while the monitor and the gpu support display modes with
pixel clocks of up to 600MHz, the link encoder might not. This prevents
YCbCr444 and RGB encoding for 4k60Hz, but YCbCr420 encoding might still be
possible. However, which color mode is used is decided before the link
encoder capabilities are checked. This patch fixes the problem by retrying
to find a display mode with YCbCr420 enforced and using it, if it is
valid.
Reviewed-by: Harry Wentland <harry.wentland@amd.com>
Signed-off-by: Werner Sembach <wse@tuxedocomputers.com>
Signed-off-by: Alex Deucher <alexander.deucher@amd.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 7d98d416c2 ]
clang points out that the %hu format string does not match the type
of the variables here:
drivers/gpu/drm/amd/amdgpu/amdgpu_uvd.c:263:7: warning: format specifies type 'unsigned short' but the argument has type 'unsigned int' [-Wformat]
version_major, version_minor);
^~~~~~~~~~~~~
include/drm/drm_print.h:498:19: note: expanded from macro 'DRM_ERROR'
__drm_err(fmt, ##__VA_ARGS__)
~~~ ^~~~~~~~~~~
Change it to a regular %u, the same way a previous patch did for
another instance of the same warning.
Reviewed-by: Christian König <christian.koenig@amd.com>
Reviewed-by: Tom Rix <trix@redhat.com>
Signed-off-by: Arnd Bergmann <arnd@arndb.de>
Signed-off-by: Alex Deucher <alexander.deucher@amd.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 54718747a6 ]
[Why]
On NAVI14 CONFIG_UBSAN reported shift-out-of-bounds at
display_rq_dlg_calc_20v2.c:304:38
rq_param->misc.rq_c.blk256_height is 0 when chroma(*_c) is invalid.
dml_log2 returns -1023 for log2(0), although log2(0) is undefined.
Which ended up as:
rq_param->dlg.rq_c.swath_height = 1 << -1023
[How]
Fix applied on all dml versions.
1. Ensure dml_log2 is only called if the argument is greater than 0.
2. Subtract req128_l/req128_c from log2_swath_height_l/log2_swath_height_c
only when it is greater than 0.
Tested-by: Daniel Wheeler <daniel.wheeler@amd.com>
Signed-off-by: Anson Jacob <Anson.Jacob@amd.com>
Reviewed-by: Dmytro Laktyushkin <Dmytro.Laktyushkin@amd.com>
Reviewed-by: Jun Lei <Jun.Lei@amd.com>
Acked-by: Solomon Chiu <solomon.chiu@amd.com>
Signed-off-by: Alex Deucher <alexander.deucher@amd.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 2ad52bdb22 ]
Leaving this at a close-to-maximum register value 0xFFF0 means it takes
very long for the MDSS to generate a software vsync interrupt when the
hardware TE interrupt doesn't arrive. Configuring this to double the
vtotal (like some downstream kernels) leads to a frame to take at most
twice before the vsync signal, until hardware TE comes up.
In this case the hardware interrupt responsible for providing this
signal - "disp-te" gpio - is not hooked up to the mdp5 vsync/pp logic at
all. This solves severe panel update issues observed on at least the
Xperia Loire and Tone series, until said gpio is properly hooked up to
an irq.
Suggested-by: AngeloGioacchino Del Regno <angelogioacchino.delregno@somainline.org>
Signed-off-by: Marijn Suijten <marijn.suijten@somainline.org>
Reviewed-by: AngeloGioacchino Del Regno <angelogioacchino.delregno@somainline.org>
Link: https://lore.kernel.org/r/20210406214726.131534-2-marijn.suijten@somainline.org
Signed-off-by: Rob Clark <robdclark@chromium.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 9bcb959d05 ]
During load balance, LBF_SOME_PINNED will be set if any candidate task
cannot be detached due to CPU affinity constraints. This can result in
setting env->sd->parent->sgc->group_imbalance, which can lead to a group
being classified as group_imbalanced (rather than any of the other, lower
group_type) when balancing at a higher level.
In workloads involving a single task per CPU, LBF_SOME_PINNED can often be
set due to per-CPU kthreads being the only other runnable tasks on any
given rq. This results in changing the group classification during
load-balance at higher levels when in reality there is nothing that can be
done for this affinity constraint: per-CPU kthreads, as the name implies,
don't get to move around (modulo hotplug shenanigans).
It's not as clear for userspace tasks - a task could be in an N-CPU cpuset
with N-1 offline CPUs, making it an "accidental" per-CPU task rather than
an intended one. KTHREAD_IS_PER_CPU gives us an indisputable signal which
we can leverage here to not set LBF_SOME_PINNED.
Note that the aforementioned classification to group_imbalance (when
nothing can be done) is especially problematic on big.LITTLE systems, which
have a topology the likes of:
DIE [ ]
MC [ ][ ]
0 1 2 3
L L B B
arch_scale_cpu_capacity(L) < arch_scale_cpu_capacity(B)
Here, setting LBF_SOME_PINNED due to a per-CPU kthread when balancing at MC
level on CPUs [0-1] will subsequently prevent CPUs [2-3] from classifying
the [0-1] group as group_misfit_task when balancing at DIE level. Thus, if
CPUs [0-1] are running CPU-bound (misfit) tasks, ill-timed per-CPU kthreads
can significantly delay the upgmigration of said misfit tasks. Systems
relying on ASYM_PACKING are likely to face similar issues.
Signed-off-by: Lingutla Chandrasekhar <clingutla@codeaurora.org>
[Use kthread_is_per_cpu() rather than p->nr_cpus_allowed]
[Reword changelog]
Signed-off-by: Valentin Schneider <valentin.schneider@arm.com>
Signed-off-by: Peter Zijlstra (Intel) <peterz@infradead.org>
Reviewed-by: Dietmar Eggemann <dietmar.eggemann@arm.com>
Reviewed-by: Vincent Guittot <vincent.guittot@linaro.org>
Link: https://lkml.kernel.org/r/20210407220628.3798191-2-valentin.schneider@arm.com
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 4f4e6644cd ]
For two of the supported sensors the stv06xx driver allocates memory which
is stored in sd->sensor_priv. This memory is freed on a disconnect, but if
the probe() fails, then it isn't freed and so this leaks memory.
Add a new probe_error() op that drivers can use to free any allocated
memory in case there was a probe failure.
Thanks to Pavel Skripkin <paskripkin@gmail.com> for discovering the cause
of the memory leak.
Reported-and-tested-by: syzbot+e7f4c64a4248a0340c37@syzkaller.appspotmail.com
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit b7cd0da982 ]
syzbot reported memory leak in dvb-usb. The problem was
in invalid error handling in dvb_usb_adapter_init().
for (n = 0; n < d->props.num_adapters; n++) {
....
if ((ret = dvb_usb_adapter_stream_init(adap)) ||
(ret = dvb_usb_adapter_dvb_init(adap, adapter_nrs)) ||
(ret = dvb_usb_adapter_frontend_init(adap))) {
return ret;
}
...
d->num_adapters_initialized++;
...
}
In case of error in dvb_usb_adapter_dvb_init() or
dvb_usb_adapter_dvb_init() d->num_adapters_initialized won't be
incremented, but dvb_usb_adapter_exit() relies on it:
for (n = 0; n < d->num_adapters_initialized; n++)
So, allocated objects won't be freed.
Signed-off-by: Pavel Skripkin <paskripkin@gmail.com>
Reported-by: syzbot+3c2be7424cea3b932b0e@syzkaller.appspotmail.com
Signed-off-by: Sean Young <sean@mess.org>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit f1995d5e43 ]
pm_runtime_get_sync() will increase the runtime PM counter
even it returns an error. Thus a pairing decrement is needed
to prevent refcount leak. Fix this by replacing this API with
pm_runtime_resume_and_get(), which will not change the runtime
PM counter on error.
Signed-off-by: Dinghao Liu <dinghao.liu@zju.edu.cn>
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 69306a947b ]
pm_runtime_get_sync() will increase the runtime PM counter
even it returns an error. Thus a pairing decrement is needed
to prevent refcount leak. Fix this by replacing this API with
pm_runtime_resume_and_get(), which will not change the runtime
PM counter on error.
Signed-off-by: Dinghao Liu <dinghao.liu@zju.edu.cn>
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 4a15275b6a ]
This driver's remove path calls cancel_delayed_work(). However, that
function does not wait until the work function finishes. This means
that the callback function may still be running after the driver's
remove function has finished, which would result in a use-after-free.
Fix by calling cancel_delayed_work_sync(), which ensures that
the work is properly cancelled, no longer running, and unable
to re-schedule itself.
Reported-by: Hulk Robot <hulkci@huawei.com>
Signed-off-by: Yang Yingliang <yangyingliang@huawei.com>
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 7f820ab5d4 ]
This driver's remove path calls cancel_delayed_work(). However, that
function does not wait until the work function finishes. This means
that the callback function may still be running after the driver's
remove function has finished, which would result in a use-after-free.
Fix by calling cancel_delayed_work_sync(), which ensures that
the work is properly cancelled, no longer running, and unable
to re-schedule itself.
Reported-by: Hulk Robot <hulkci@huawei.com>
Signed-off-by: Yang Yingliang <yangyingliang@huawei.com>
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 2c9541720c ]
This driver's remove path calls cancel_delayed_work(). However, that
function does not wait until the work function finishes. This means
that the callback function may still be running after the driver's
remove function has finished, which would result in a use-after-free.
Fix by calling cancel_delayed_work_sync(), which ensures that
the work is properly cancelled, no longer running, and unable
to re-schedule itself.
Reported-by: Hulk Robot <hulkci@huawei.com>
Signed-off-by: Yang Yingliang <yangyingliang@huawei.com>
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit fa56f5f1fe ]
This driver's remove path calls cancel_delayed_work(). However, that
function does not wait until the work function finishes. This means
that the callback function may still be running after the driver's
remove function has finished, which would result in a use-after-free.
Fix by calling cancel_delayed_work_sync(), which ensures that
the work is properly cancelled, no longer running, and unable
to re-schedule itself.
Reported-by: Hulk Robot <hulkci@huawei.com>
Signed-off-by: Yang Yingliang <yangyingliang@huawei.com>
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 6107a4fdf8 ]
This driver's remove path calls cancel_delayed_work(). However, that
function does not wait until the work function finishes. This means
that the callback function may still be running after the driver's
remove function has finished, which would result in a use-after-free.
Fix by calling cancel_delayed_work_sync(), which ensures that
the work is properly cancelled, no longer running, and unable
to re-schedule itself.
Reported-by: Hulk Robot <hulkci@huawei.com>
Signed-off-by: Yang Yingliang <yangyingliang@huawei.com>
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 68ae256945 ]
This driver's remove path calls cancel_delayed_work(). However, that
function does not wait until the work function finishes. This means
that the callback function may still be running after the driver's
remove function has finished, which would result in a use-after-free.
Fix by calling cancel_delayed_work_sync(), which ensures that
the work is properly cancelled, no longer running, and unable
to re-schedule itself.
Reported-by: Hulk Robot <hulkci@huawei.com>
Signed-off-by: Yang Yingliang <yangyingliang@huawei.com>
Reviewed-by: Krzysztof Kozlowski <krzysztof.kozlowski@canonical.com>
Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit b6cfa007b3 ]
This driver's remove path calls cancel_delayed_work(). However, that
function does not wait until the work function finishes. This means
that the callback function may still be running after the driver's
remove function has finished, which would result in a use-after-free.
Fix by calling cancel_delayed_work_sync(), which ensures that
the work is properly cancelled, no longer running, and unable
to re-schedule itself.
Reported-by: Hulk Robot <hulkci@huawei.com>
Signed-off-by: Yang Yingliang <yangyingliang@huawei.com>
Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 443ec4bbc6 ]
The EDID had a few mistakes as reported by edid-decode:
Block 1, CTA-861 Extension Block:
Video Data Block: For improved preferred timing interoperability, set 'Native detailed modes' to 1.
Video Capability Data Block: S_PT is equal to S_IT and S_CE, so should be set to 0 instead.
Fixed those.
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 0ae10a7dc8 ]
If some error occurs, URB buffers should also be freed. If they aren't
freed with the dvb here, the em28xx_dvb_fini call doesn't frees the URB
buffers as dvb is set to NULL. The function in which error occurs should
do all the cleanup for the allocations it had done.
Tested the patch with the reproducer provided by syzbot. This patch
fixes the memleak.
Reported-by: syzbot+889397c820fa56adf25d@syzkaller.appspotmail.com
Signed-off-by: Muhammad Usama Anjum <musamaanjum@gmail.com>
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>