[ Upstream commit 7fbf6b731b ]
Interrupt line can be configured on different hardware in different way,
even inverted. Therefore driver should not enforce specific trigger
type - edge falling - but instead rely on Devicetree to configure it.
The Maxim 17047/77693 datasheets describe the interrupt line as active
low with a requirement of acknowledge from the CPU therefore the edge
falling is not correct.
The interrupt line is shared between PMIC and RTC driver, so using level
sensitive interrupt is here especially important to avoid races. With
an edge configuration in case if first PMIC signals interrupt followed
shortly after by the RTC, the interrupt might not be yet cleared/acked
thus the second one would not be noticed.
Signed-off-by: Krzysztof Kozlowski <krzk@kernel.org>
Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 5bcb5087c9 ]
Sometimes the code will crash because we haven't enabled
AC or USB charging and thus not created the corresponding
psy device. Fix it by checking that it is there before
notifying.
Signed-off-by: Linus Walleij <linus.walleij@linaro.org>
Signed-off-by: Sebastian Reichel <sebastian.reichel@collabora.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit b601a18f12 ]
A consumer is expected to disable a PWM before calling pwm_put(). And if
they didn't there is hopefully a good reason (or the consumer needs
fixing). Also if disabling an enabled PWM was the right thing to do,
this should better be done in the framework instead of in each low level
driver.
So drop the hardware modification from the .remove() callback.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Signed-off-by: Thierry Reding <thierry.reding@gmail.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 2c484419ef ]
lz4 compatible decompressor is simple. The format is underspecified and
relies on EOF notification to determine when to stop. Initramfs buffer
format[1] explicitly states that it can have arbitrary number of zero
padding. Thus when operating without a fill function, be extra careful to
ensure that sizes less than 4, or apperantly empty chunksizes are treated
as EOF.
To test this I have created two cpio initrds, first a normal one,
main.cpio. And second one with just a single /test-file with content
"second" second.cpio. Then i compressed both of them with gzip, and with
lz4 -l. Then I created a padding of 4 bytes (dd if=/dev/zero of=pad4 bs=1
count=4). To create four testcase initrds:
1) main.cpio.gzip + extra.cpio.gzip = pad0.gzip
2) main.cpio.lz4 + extra.cpio.lz4 = pad0.lz4
3) main.cpio.gzip + pad4 + extra.cpio.gzip = pad4.gzip
4) main.cpio.lz4 + pad4 + extra.cpio.lz4 = pad4.lz4
The pad4 test-cases replicate the initrd load by grub, as it pads and
aligns every initrd it loads.
All of the above boot, however /test-file was not accessible in the initrd
for the testcase #4, as decoding in lz4 decompressor failed. Also an
error message printed which usually is harmless.
Whith a patched kernel, all of the above testcases now pass, and
/test-file is accessible.
This fixes lz4 initrd decompress warning on every boot with grub. And
more importantly this fixes inability to load multiple lz4 compressed
initrds with grub. This patch has been shipping in Ubuntu kernels since
January 2021.
[1] ./Documentation/driver-api/early-userspace/buffer-format.rst
BugLink: https://bugs.launchpad.net/bugs/1835660
Link: https://lore.kernel.org/lkml/20210114200256.196589-1-xnox@ubuntu.com/ # v0
Link: https://lkml.kernel.org/r/20210513104831.432975-1-dimitri.ledkov@canonical.com
Signed-off-by: Dimitri John Ledkov <dimitri.ledkov@canonical.com>
Cc: Kyungsik Lee <kyungsik.lee@lge.com>
Cc: Yinghai Lu <yinghai@kernel.org>
Cc: Bongkyu Kim <bongkyu.kim@lge.com>
Cc: Kees Cook <keescook@chromium.org>
Cc: Sven Schmidt <4sschmid@informatik.uni-hamburg.de>
Cc: Rajat Asthana <thisisrast7@gmail.com>
Cc: Nick Terrell <terrelln@fb.com>
Cc: Gao Xiang <hsiangkao@redhat.com>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit b64210f2f7 ]
If an i2c client receives an interrupt during reboot or shutdown it may
be too late to service it by making an i2c transaction on the bus
because the i2c controller has already been shutdown. This can lead to
system hangs if the i2c controller tries to make a transfer that is
doomed to fail because the access to the i2c pins is already shut down,
or an iommu translation has been torn down so i2c controller register
access doesn't work.
Let's simply disable the irq if there isn't a shutdown callback for an
i2c client when there is an irq associated with the device. This will
make sure that irqs don't come in later than the time that we can handle
it. We don't do this if the i2c client device already has a shutdown
callback because presumably they're doing the right thing and quieting
the device so irqs don't come in after the shutdown callback returns.
Reported-by: kernel test robot <lkp@intel.com>
[swboyd@chromium.org: Dropped newline, added commit text, added
interrupt.h for robot build error]
Signed-off-by: Stephen Boyd <swboyd@chromium.org>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
Signed-off-by: Wolfram Sang <wsa@kernel.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit b9481a667a ]
According to <linux/backlight.h> .update_status() is supposed to
return 0 on success and a negative error code otherwise. Adapt
lm3630a_bank_a_update_status() and lm3630a_bank_b_update_status() to
actually do it.
While touching that also add the error code to the failure message.
Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de>
Reviewed-by: Daniel Thompson <daniel.thompson@linaro.org>
Signed-off-by: Lee Jones <lee.jones@linaro.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 50ebe56222 ]
A user of FFADO project reported the issue of ToneWeal FW66. As a result,
the device is identified as one of applications of BeBoB solution.
I note that in the report the device returns contradictory result in plug
discovery process for audio subunit. Fortunately ALSA BeBoB driver doesn't
perform it thus it's likely to handle the device without issues.
I receive no reaction to test request for this patch yet, however it would
be worth to add support for it.
daniel@gibbonmoon:/sys/bus/firewire/devices/fw1$ grep -r . *
Binary file config_rom matches
dev:244:1
guid:0x0023270002000000
hardware_version:0x000002
is_local:0
model:0x020002
model_name:FW66
power/runtime_active_time:0
power/runtime_active_kids:0
power/runtime_usage:0
power/runtime_status:unsupported
power/async:disabled
power/runtime_suspended_time:0
power/runtime_enabled:disabled
power/control:auto
subsystem/drivers_autoprobe:1
uevent:MAJOR=244
uevent:MINOR=1
uevent:DEVNAME=fw1
units:0x00a02d:0x010001
vendor:0x002327
vendor_name:ToneWeal
fw1.0/uevent:MODALIAS=ieee1394:ven00002327mo00020002sp0000A02Dver00010001
fw1.0/power/runtime_active_time:0
fw1.0/power/runtime_active_kids:0
fw1.0/power/runtime_usage:0
fw1.0/power/runtime_status:unsupported
fw1.0/power/async:disabled
fw1.0/power/runtime_suspended_time:0
fw1.0/power/runtime_enabled:disabled
fw1.0/power/control:auto
fw1.0/model:0x020002
fw1.0/rom_index:15
fw1.0/specifier_id:0x00a02d
fw1.0/model_name:FW66
fw1.0/version:0x010001
fw1.0/modalias:ieee1394:ven00002327mo00020002sp0000A02Dver00010001
Cc: Daniel Jozsef <daniel.jozsef@gmail.com>
Reference: https://lore.kernel.org/alsa-devel/20200119164335.GA11974@workstation/
Signed-off-by: Takashi Sakamoto <o-takashi@sakamocchi.jp>
Link: https://lore.kernel.org/r/20210619083922.16060-1-o-takashi@sakamocchi.jp
Signed-off-by: Takashi Iwai <tiwai@suse.de>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit cac7100d4c ]
Inside function hideep_nvm_unlock(), variable "unmask_code" could
be uninitialized if hideep_pgm_r_reg() returns error, however, it
is used in the later if statement after an "and" operation, which
is potentially unsafe.
Signed-off-by: Yizhuo <yzhai003@ucr.edu>
Signed-off-by: Dmitry Torokhov <dmitry.torokhov@gmail.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 6d49b3a0f3 ]
The On Semi pca9655 is a 16 bit variant of the On Semi pca9654 GPIO
expander, with 16 GPIOs and interrupt functionality.
Signed-off-by: Peter Robinson <pbrobinson@gmail.com>
[Bartosz: fixed indentation as noted by Andy]
Signed-off-by: Bartosz Golaszewski <bgolaszewski@baylibre.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 45677c9aeb ]
The "no_handler_test" in ebb selftests attempts to read the PMU
registers twice via helper function "dump_ebb_state". First dump is
just before closing of event and the second invocation is done after
closing of the event. The original intention of second
dump_ebb_state was to dump the state of registers at the end of
the test when the counters are frozen. But this will be achieved
with the first call itself since sample period is set to low value
and PMU will be frozen by then. Hence patch removes the
dump which was done before closing of the event.
Reported-by: Shirisha Ganta <shirisha.ganta1@ibm.com>
Signed-off-by: Athira Rajeev <atrajeev@linux.vnet.ibm.com>
Tested-by: Nageswara R Sastry <rnsastry@linux.ibm.com <mailto:rnsastry@linux.ibm.com>>
Signed-off-by: Michael Ellerman <mpe@ellerman.id.au>
Link: https://lore.kernel.org/r/1621950703-1532-2-git-send-email-atrajeev@linux.vnet.ibm.com
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit a51b2fb94b ]
Return value of "pm_runtime_get_sync" API was neither captured nor checked.
Fixed it by capturing the return value and then checking for any warning.
Addresses-Coverity: "check_return"
Signed-off-by: Srinivas Neeli <srinivas.neeli@xilinx.com>
Signed-off-by: Bartosz Golaszewski <bgolaszewski@baylibre.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 9733862e50 ]
Commit f959dcd6dd (dma-direct: Fix
potential NULL pointer dereference) added a null check on the
dma_mask pointer of the kernel's device structure.
Add a dma_mask variable to the ps3_dma_region structure and set
the device structure's dma_mask pointer to point to this new variable.
Fixes runtime errors like these:
# WARNING: Fixes tag on line 10 doesn't match correct format
# WARNING: Fixes tag on line 10 doesn't match correct format
ps3_system_bus_match:349: dev=8.0(sb_01), drv=8.0(ps3flash): match
WARNING: CPU: 0 PID: 1 at kernel/dma/mapping.c:151 .dma_map_page_attrs+0x34/0x1e0
ps3flash sb_01: ps3stor_setup:193: map DMA region failed
Signed-off-by: Geoff Levand <geoff@infradead.org>
Signed-off-by: Michael Ellerman <mpe@ellerman.id.au>
Link: https://lore.kernel.org/r/562d0c9ea0100a30c3b186bcc7adb34b0bbd2cd7.1622746428.git.geoff@infradead.org
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit c305366a37 ]
snd_sb_qsound_destroy() contains the calls of removing the previously
created mixer controls, but it doesn't clear the pointers. As
snd_sb_qsound_destroy() itself may be repeatedly called via ioctl,
this could lead to double-free potentially.
Fix it by clearing the struct fields properly afterwards.
Link: https://lore.kernel.org/r/20210608140540.17885-4-tiwai@suse.de
Signed-off-by: Takashi Iwai <tiwai@suse.de>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 0d3e5a0579 ]
This test will require /dev/rtc0, the default RTC device, or one
specified by user to run. Since this default RTC is not guaranteed to
exist on all of the devices, so check its existence first, otherwise
skip this test with the kselftest skip code 4.
Without this patch this test will fail like this on a s390x zVM:
$ selftests: timers: rtcpie
$ /dev/rtc0: No such file or directory
not ok 1 selftests: timers: rtcpie # exit=22
With this patch:
$ selftests: timers: rtcpie
$ Default RTC /dev/rtc0 does not exist. Test Skipped!
not ok 9 selftests: timers: rtcpie # SKIP
Fixed up change log so "With this patch" text doesn't get dropped.
Shuah Khan <skhan@linuxfoundation.org>
Signed-off-by: Po-Hsu Lin <po-hsu.lin@canonical.com>
Signed-off-by: Shuah Khan <skhan@linuxfoundation.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 4700ef3265 ]
This patch adds/modifies MODULE_DEVICE_TABLE definition which generates
correct modalias for automatic loading of this driver when it is built
as an external module.
Reported-by: Hulk Robot <hulkci@huawei.com>
Signed-off-by: Zou Wei <zou_wei@huawei.com>
Signed-off-by: Lee Jones <lee.jones@linaro.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit bdd4aad7ff ]
The iscsi offload drivers are setting the shost->max_id to the max number
of sessions they support. The problem is that max_id is not the max number
of targets but the highest identifier the targets can have. To use it to
limit the number of targets we need to set it to max sessions - 1, or we
can end up with a session we might not have preallocated resources for.
Link: https://lore.kernel.org/r/20210525181821.7617-15-michael.christie@oracle.com
Reviewed-by: Lee Duncan <lduncan@suse.com>
Signed-off-by: Mike Christie <michael.christie@oracle.com>
Signed-off-by: Martin K. Petersen <martin.petersen@oracle.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit ec29d0ac29 ]
If we haven't done a unbind target call we can race where
iscsi_conn_teardown wakes up the EH thread and then frees the conn while
those threads are still accessing the conn ehwait.
We can only do one TMF per session so this just moves the TMF fields from
the conn to the session. We can then rely on the
iscsi_session_teardown->iscsi_remove_session->__iscsi_unbind_session call
to remove the target and it's devices, and know after that point there is
no device or scsi-ml callout trying to access the session.
Link: https://lore.kernel.org/r/20210525181821.7617-14-michael.christie@oracle.com
Reviewed-by: Lee Duncan <lduncan@suse.com>
Signed-off-by: Mike Christie <michael.christie@oracle.com>
Signed-off-by: Martin K. Petersen <martin.petersen@oracle.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit e30d55137e ]
An 'unexpected timeout' message may be seen in a point-2-point topology.
The message occurs when a PLOGI is received before the driver is notified
of FLOGI completion. The FLOGI completion failure causes discovery to be
triggered for a second time. The discovery timer is restarted but no new
discovery activity is initiated, thus the timeout message eventually
appears.
In point-2-point, when discovery has progressed before the FLOGI completion
is processed, it is not a failure. Add code to FLOGI completion to detect
that discovery has progressed and exit the FLOGI handling (noop'ing it).
Link: https://lore.kernel.org/r/20210514195559.119853-4-jsmart2021@gmail.com
Co-developed-by: Justin Tee <justin.tee@broadcom.com>
Signed-off-by: Justin Tee <justin.tee@broadcom.com>
Signed-off-by: James Smart <jsmart2021@gmail.com>
Signed-off-by: Martin K. Petersen <martin.petersen@oracle.com>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 5d6fb80a14 ]
This reverts commit 0edabdfe89.
I've explained that optional FireWire card for d.2 is also built-in to
d.2 Pro, however it's wrong. The optional card uses DM1000 ASIC and has
'Mackie DJ Mixer' in its model name of configuration ROM. On the other
hand, built-in FireWire card for d.2 Pro and d.4 Pro uses OXFW971 ASIC
and has 'd.Pro' in its model name according to manuals and user
experiences. The former card is not the card for d.2 Pro. They are similar
in appearance but different internally.
Signed-off-by: Takashi Sakamoto <o-takashi@sakamocchi.jp>
Link: https://lore.kernel.org/r/20210518084557.102681-2-o-takashi@sakamocchi.jp
Signed-off-by: Takashi Iwai <tiwai@suse.de>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 7272b591c4 ]
In ibmasm_init_one, it calls ibmasm_init_remote_input_dev().
Inside ibmasm_init_remote_input_dev, mouse_dev and keybd_dev are
allocated by input_allocate_device(), and assigned to
sp->remote.mouse_dev and sp->remote.keybd_dev respectively.
In the err_free_devices error branch of ibmasm_init_one,
mouse_dev and keybd_dev are freed by input_free_device(), and return
error. Then the execution runs into error_send_message error branch
of ibmasm_init_one, where ibmasm_free_remote_input_dev(sp) is called
to unregister the freed sp->remote.mouse_dev and sp->remote.keybd_dev.
My patch add a "error_init_remote" label to handle the error of
ibmasm_init_remote_input_dev(), to avoid the uaf bugs.
Signed-off-by: Lv Yunlong <lyl2019@mail.ustc.edu.cn>
Link: https://lore.kernel.org/r/20210426170620.10546-1-lyl2019@mail.ustc.edu.cn
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit fcb10ee27f ]
We should be very careful about the register values that will be used
for division or modulo operations, althrough the possibility that the
UARTBAUD register value is zero is very low, but we had better to deal
with the "bad data" of hardware in advance to avoid division or modulo
by zero leading to undefined kernel behavior.
Signed-off-by: Sherry Sun <sherry.sun@nxp.com>
Link: https://lore.kernel.org/r/20210427021226.27468-1-sherry.sun@nxp.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Signed-off-by: Sasha Levin <sashal@kernel.org>
commit f18139966d upstream.
Trying to start a new PIO transfer by writing value 0 in PIO_START register
when previous transfer has not yet completed (which is indicated by value 1
in PIO_START) causes an External Abort on CPU, which results in kernel
panic:
SError Interrupt on CPU0, code 0xbf000002 -- SError
Kernel panic - not syncing: Asynchronous SError Interrupt
To prevent kernel panic, it is required to reject a new PIO transfer when
previous one has not finished yet.
If previous PIO transfer is not finished yet, the kernel may issue a new
PIO request only if the previous PIO transfer timed out.
In the past the root cause of this issue was incorrectly identified (as it
often happens during link retraining or after link down event) and special
hack was implemented in Trusted Firmware to catch all SError events in EL3,
to ignore errors with code 0xbf000002 and not forwarding any other errors
to kernel and instead throw panic from EL3 Trusted Firmware handler.
Links to discussion and patches about this issue:
https://git.trustedfirmware.org/TF-A/trusted-firmware-a.git/commit/?id=3c7dcdac5c50https://lore.kernel.org/linux-pci/20190316161243.29517-1-repk@triplefau.lt/https://lore.kernel.org/linux-pci/971be151d24312cc533989a64bd454b4@www.loen.fr/https://review.trustedfirmware.org/c/TF-A/trusted-firmware-a/+/1541
But the real cause was the fact that during link retraining or after link
down event the PIO transfer may take longer time, up to the 1.44s until it
times out. This increased probability that a new PIO transfer would be
issued by kernel while previous one has not finished yet.
After applying this change into the kernel, it is possible to revert the
mentioned TF-A hack and SError events do not have to be caught in TF-A EL3.
Link: https://lore.kernel.org/r/20210608203655.31228-1-pali@kernel.org
Signed-off-by: Pali Rohár <pali@kernel.org>
Signed-off-by: Lorenzo Pieralisi <lorenzo.pieralisi@arm.com>
Signed-off-by: Bjorn Helgaas <bhelgaas@google.com>
Reviewed-by: Marek Behún <kabel@kernel.org>
Cc: stable@vger.kernel.org # 7fbcb5da81 ("PCI: aardvark: Don't rely on jiffies while holding spinlock")
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 7fbcb5da81 upstream.
advk_pcie_wait_pio() can be called while holding a spinlock (from
pci_bus_read_config_dword()), then depends on jiffies in order to
timeout while polling on PIO state registers. In the case the PIO
transaction failed, the timeout will never happen and will also cause
the cpu to stall.
This decrements a variable and wait instead of using jiffies.
Signed-off-by: Remi Pommarel <repk@triplefau.lt>
Signed-off-by: Lorenzo Pieralisi <lorenzo.pieralisi@arm.com>
Reviewed-by: Andrew Murray <andrew.murray@arm.com>
Acked-by: Thomas Petazzoni <thomas.petazzoni@bootlin.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 93aa71ad73 upstream.
Commit 66a834d092 ("scsi: core: Fix error handling of scsi_host_alloc()")
changed the allocation logic to call put_device() to perform host cleanup
with the assumption that IDA removal and stopping the kthread would
properly be performed in scsi_host_dev_release(). However, in the unlikely
case that the error handler thread fails to spawn, shost->ehandler is set
to ERR_PTR(-ENOMEM).
The error handler cleanup code in scsi_host_dev_release() will call
kthread_stop() if shost->ehandler != NULL which will always be the case
whether the kthread was successfully spawned or not. In the case that it
failed to spawn this has the nasty side effect of trying to dereference an
invalid pointer when kthread_stop() is called. The following splat provides
an example of this behavior in the wild:
scsi host11: error handler thread failed to spawn, error = -4
Kernel attempted to read user page (10c) - exploit attempt? (uid: 0)
BUG: Kernel NULL pointer dereference on read at 0x0000010c
Faulting instruction address: 0xc00000000818e9a8
Oops: Kernel access of bad area, sig: 11 [#1]
LE PAGE_SIZE=64K MMU=Hash SMP NR_CPUS=2048 NUMA pSeries
Modules linked in: ibmvscsi(+) scsi_transport_srp dm_multipath dm_mirror dm_region
hash dm_log dm_mod fuse overlay squashfs loop
CPU: 12 PID: 274 Comm: systemd-udevd Not tainted 5.13.0-rc7 #1
NIP: c00000000818e9a8 LR: c0000000089846e8 CTR: 0000000000007ee8
REGS: c000000037d12ea0 TRAP: 0300 Not tainted (5.13.0-rc7)
MSR: 800000000280b033 <SF,VEC,VSX,EE,FP,ME,IR,DR,RI,LE> CR: 28228228
XER: 20040001
CFAR: c0000000089846e4 DAR: 000000000000010c DSISR: 40000000 IRQMASK: 0
GPR00: c0000000089846e8 c000000037d13140 c000000009cc1100 fffffffffffffffc
GPR04: 0000000000000001 0000000000000000 0000000000000000 c000000037dc0000
GPR08: 0000000000000000 c000000037dc0000 0000000000000001 00000000fffff7ff
GPR12: 0000000000008000 c00000000a049000 c000000037d13d00 000000011134d5a0
GPR16: 0000000000001740 c0080000190d0000 c0080000190d1740 c000000009129288
GPR20: c000000037d13bc0 0000000000000001 c000000037d13bc0 c0080000190b7898
GPR24: c0080000190b7708 0000000000000000 c000000033bb2c48 0000000000000000
GPR28: c000000046b28280 0000000000000000 000000000000010c fffffffffffffffc
NIP [c00000000818e9a8] kthread_stop+0x38/0x230
LR [c0000000089846e8] scsi_host_dev_release+0x98/0x160
Call Trace:
[c000000033bb2c48] 0xc000000033bb2c48 (unreliable)
[c0000000089846e8] scsi_host_dev_release+0x98/0x160
[c00000000891e960] device_release+0x60/0x100
[c0000000087e55c4] kobject_release+0x84/0x210
[c00000000891ec78] put_device+0x28/0x40
[c000000008984ea4] scsi_host_alloc+0x314/0x430
[c0080000190b38bc] ibmvscsi_probe+0x54/0xad0 [ibmvscsi]
[c000000008110104] vio_bus_probe+0xa4/0x4b0
[c00000000892a860] really_probe+0x140/0x680
[c00000000892aefc] driver_probe_device+0x15c/0x200
[c00000000892b63c] device_driver_attach+0xcc/0xe0
[c00000000892b740] __driver_attach+0xf0/0x200
[c000000008926f28] bus_for_each_dev+0xa8/0x130
[c000000008929ce4] driver_attach+0x34/0x50
[c000000008928fc0] bus_add_driver+0x1b0/0x300
[c00000000892c798] driver_register+0x98/0x1a0
[c00000000810eb60] __vio_register_driver+0x80/0xe0
[c0080000190b4a30] ibmvscsi_module_init+0x9c/0xdc [ibmvscsi]
[c0000000080121d0] do_one_initcall+0x60/0x2d0
[c000000008261abc] do_init_module+0x7c/0x320
[c000000008265700] load_module+0x2350/0x25b0
[c000000008265cb4] __do_sys_finit_module+0xd4/0x160
[c000000008031110] system_call_exception+0x150/0x2d0
[c00000000800d35c] system_call_common+0xec/0x278
Fix this be nulling shost->ehandler when the kthread fails to spawn.
Link: https://lore.kernel.org/r/20210701195659.3185475-1-tyreld@linux.ibm.com
Fixes: 66a834d092 ("scsi: core: Fix error handling of scsi_host_alloc()")
Cc: stable@vger.kernel.org
Reviewed-by: Ming Lei <ming.lei@redhat.com>
Signed-off-by: Tyrel Datwyler <tyreld@linux.ibm.com>
Signed-off-by: Martin K. Petersen <martin.petersen@oracle.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit f85d401606 upstream.
When the host is using debug registers but the guest is not using them
nor is the guest in guest-debug state, the kvm code does not reset
the host debug registers before kvm_x86->run(). Rather, it relies on
the hardware vmentry instruction to automatically reset the dr7 registers
which ensures that the host breakpoints do not affect the guest.
This however violates the non-instrumentable nature around VM entry
and exit; for example, when a host breakpoint is set on vcpu->arch.cr2,
Another issue is consistency. When the guest debug registers are active,
the host breakpoints are reset before kvm_x86->run(). But when the
guest debug registers are inactive, the host breakpoints are delayed to
be disabled. The host tracing tools may see different results depending
on what the guest is doing.
To fix the problems, we clear %db7 unconditionally before kvm_x86->run()
if the host has set any breakpoints, no matter if the guest is using
them or not.
Signed-off-by: Lai Jiangshan <laijs@linux.alibaba.com>
Message-Id: <20210628172632.81029-1-jiangshanlai@gmail.com>
Cc: stable@vger.kernel.org
[Only clear %db7 instead of reloading all debug registers. - Paolo]
Signed-off-by: Paolo Bonzini <pbonzini@redhat.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 4bf48e3c0a upstream.
Ignore the guest MAXPHYADDR reported by CPUID.0x8000_0008 if TDP, i.e.
NPT, is disabled, and instead use the host's MAXPHYADDR. Per AMD'S APM:
Maximum guest physical address size in bits. This number applies only
to guests using nested paging. When this field is zero, refer to the
PhysAddrSize field for the maximum guest physical address size.
Fixes: 24c82e576b ("KVM: Sanitize cpuid")
Cc: stable@vger.kernel.org
Signed-off-by: Sean Christopherson <seanjc@google.com>
Message-Id: <20210623230552.4027702-2-seanjc@google.com>
Signed-off-by: Paolo Bonzini <pbonzini@redhat.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 4c6e097629 upstream.
The Elgato Cam Link 4K HDMI video capture card reports to support three
different pixel formats, where the first format depends on the connected
HDMI device.
```
$ v4l2-ctl -d /dev/video0 --list-formats-ext
ioctl: VIDIOC_ENUM_FMT
Type: Video Capture
[0]: 'NV12' (Y/CbCr 4:2:0)
Size: Discrete 3840x2160
Interval: Discrete 0.033s (29.970 fps)
[1]: 'NV12' (Y/CbCr 4:2:0)
Size: Discrete 3840x2160
Interval: Discrete 0.033s (29.970 fps)
[2]: 'YU12' (Planar YUV 4:2:0)
Size: Discrete 3840x2160
Interval: Discrete 0.033s (29.970 fps)
```
Changing the pixel format to anything besides the first pixel format
does not work:
```
$ v4l2-ctl -d /dev/video0 --try-fmt-video pixelformat=YU12
Format Video Capture:
Width/Height : 3840/2160
Pixel Format : 'NV12' (Y/CbCr 4:2:0)
Field : None
Bytes per Line : 3840
Size Image : 12441600
Colorspace : sRGB
Transfer Function : Rec. 709
YCbCr/HSV Encoding: Rec. 709
Quantization : Default (maps to Limited Range)
Flags :
```
User space applications like VLC might show an error message on the
terminal in that case:
```
libv4l2: error set_fmt gave us a different result than try_fmt!
```
Depending on the error handling of the user space applications, they
might display a distorted video, because they use the wrong pixel format
for decoding the stream.
The Elgato Cam Link 4K responds to the USB video probe
VS_PROBE_CONTROL/VS_COMMIT_CONTROL with a malformed data structure: The
second byte contains bFormatIndex (instead of being the second byte of
bmHint). The first byte is always zero. The third byte is always 1.
The firmware bug was reported to Elgato on 2020-12-01 and it was
forwarded by the support team to the developers as feature request.
There is no firmware update available since then. The latest firmware
for Elgato Cam Link 4K as of 2021-03-23 has MCU 20.02.19 and FPGA 67.
Therefore correct the malformed data structure for this device. The
change was successfully tested with VLC, OBS, and Chromium using
different pixel formats (YUYV, NV12, YU12), resolutions (3840x2160,
1920x1080), and frame rates (29.970 and 59.940 fps).
Cc: stable@vger.kernel.org
Signed-off-by: Benjamin Drung <bdrung@posteo.de>
Signed-off-by: Laurent Pinchart <laurent.pinchart@ideasonboard.com>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit b4bb4d425b upstream.
The direction of the pipe argument must match the request-type direction
bit or control requests may fail depending on the host-controller-driver
implementation.
Control transfers without a data stage are treated as OUT requests by
the USB stack and should be using usb_sndctrlpipe(). Failing to do so
will now trigger a warning.
Fix the single zero-length control request which was using the
read-register helper, and update the helper so that zero-length reads
fail with an error message instead.
Fixes: 6a7eba24e4 ("V4L/DVB (8157): gspca: all subdrivers")
Cc: stable@vger.kernel.org # 2.6.27
Signed-off-by: Johan Hovold <johan@kernel.org>
Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl>
Signed-off-by: Mauro Carvalho Chehab <mchehab+huawei@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>