commit 04ec4e6250 upstream.
Martyn Welch reports that his CPU port is unable to link where it has
been necessary to use one of the switch ports with an internal PHY for
the CPU port. The reason behind this is the port control register is
left forcing the link down, preventing traffic flow.
This occurs because during initialisation, phylink expects the link to
be down, and DSA forces the link down by synthesising a call to the
DSA drivers phylink_mac_link_down() method, but we don't touch the
forced-link state when we later reconfigure the port.
Resolve this by also unforcing the link state when we are operating in
PHY mode and the PPU is set to poll the PHY to retrieve link status
information.
Reported-by: Martyn Welch <martyn.welch@collabora.com>
Tested-by: Martyn Welch <martyn.welch@collabora.com>
Fixes: 3be98b2d5f ("net: dsa: Down cpu/dsa ports phylink will control")
Cc: <stable@vger.kernel.org> # 5.7: 2b29cb9e3f: net: dsa: mv88e6xxx: fix "don't use PHY_DETECT on internal PHY's"
Signed-off-by: Russell King (Oracle) <rmk+kernel@armlinux.org.uk>
Link: https://lore.kernel.org/r/E1mvFhP-00F8Zb-Ul@rmk-PC.armlinux.org.uk
Signed-off-by: Jakub Kicinski <kuba@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 2b29cb9e3f upstream.
This commit fixes a misunderstanding in commit 4a3e0aeddf ("net: dsa:
mv88e6xxx: don't use PHY_DETECT on internal PHY's").
For Marvell DSA switches with the PHY_DETECT bit (for non-6250 family
devices), controls whether the PPU polls the PHY to retrieve the link,
speed, duplex and pause status to update the port configuration. This
applies for both internal and external PHYs.
For some switches such as 88E6352 and 88E6390X, PHY_DETECT has an
additional function of enabling auto-media mode between the internal
PHY and SERDES blocks depending on which first gains link.
The original intention of commit 5d5b231da7 (net: dsa: mv88e6xxx: use
PHY_DETECT in mac_link_up/mac_link_down) was to allow this bit to be
used to detect when this propagation is enabled, and allow software to
update the port configuration. This has found to be necessary for some
switches which do not automatically propagate status from the SERDES to
the port, which includes the 88E6390. However, commit 4a3e0aeddf
("net: dsa: mv88e6xxx: don't use PHY_DETECT on internal PHY's") breaks
this assumption.
Maarten Zanders has confirmed that the issue he was addressing was for
an 88E6250 switch, which does not have a PHY_DETECT bit in bit 12, but
instead a link status bit. Therefore, mv88e6xxx_port_ppu_updates() does
not report correctly.
This patch resolves the above issues by reverting Maarten's change and
instead making mv88e6xxx_port_ppu_updates() indicate whether the port
is internal for the 88E6250 family of switches.
Yes, you're right, I'm targeting the 6250 family. And yes, your
suggestion would solve my case and is a better implementation for
the other devices (as far as I can see).
Fixes: 4a3e0aeddf ("net: dsa: mv88e6xxx: don't use PHY_DETECT on internal PHY's")
Signed-off-by: Russell King <rmk+kernel@armlinux.org.uk>
Tested-by: Maarten Zanders <maarten.zanders@mind.be>
Link: https://lore.kernel.org/r/E1muXm7-00EwJB-7n@rmk-PC.armlinux.org.uk
Signed-off-by: Jakub Kicinski <kuba@kernel.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit f58ac1adc7 upstream.
With the design of this driver, this condition is often triggered.
However, the counter that this interrupt indicates an overflow is never
read either, so overflowing is harmless.
On my system, when a CAN bus starts flapping up and down, this locks up
the whole system with lots of interrupts and printks.
Specifically, this interrupt indicates the CEL field of ECR has
overflowed. All reads of ECR mask out CEL.
Fixes: e0d1f4816f ("can: m_can: add Bosch M_CAN controller support")
Link: https://lore.kernel.org/all/20211129222628.7490-1-brian.silverman@bluerivertech.com
Cc: stable@vger.kernel.org
Signed-off-by: Brian Silverman <brian.silverman@bluerivertech.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 31cb32a590 upstream.
In m_can_read_fifo(), if the second call to m_can_fifo_read() fails,
the function jump to the out_fail label and returns without calling
m_can_receive_skb(). This means that the skb previously allocated by
alloc_can_skb() is not freed. In other terms, this is a memory leak.
This patch adds a goto label to destroy the skb if an error occurs.
Issue was found with GCC -fanalyzer, please follow the link below for
details.
Fixes: e39381770e ("can: m_can: Disable IRQs on FIFO bus errors")
Link: https://lore.kernel.org/all/20211107050755.70655-1-mailhol.vincent@wanadoo.fr
Cc: stable@vger.kernel.org
Cc: Matt Kline <matt@bitbashing.io>
Signed-off-by: Vincent Mailhol <mailhol.vincent@wanadoo.fr>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit fb12797ab1 upstream.
The CAN clock frequency is used when calculating the CAN bittiming
parameters. When wrong clock frequency is used, the device may end up
with wrong bittiming parameters, depending on user requested bittiming
parameters.
To avoid this, get the CAN clock frequency from the device. Various
existing Kvaser Leaf products use different CAN clocks.
Fixes: 080f40a6fa ("can: kvaser_usb: Add support for Kvaser CAN/USB devices")
Link: https://lore.kernel.org/all/20211208152122.250852-2-extja@kvaser.com
Cc: stable@vger.kernel.org
Signed-off-by: Jimmy Assarsson <extja@kvaser.com>
Signed-off-by: Marc Kleine-Budde <mkl@pengutronix.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 60a8b5a161 upstream.
This buffer is currently allocated in hfi1_init():
if (reinit)
ret = init_after_reset(dd);
else
ret = loadtime_init(dd);
if (ret)
goto done;
/* allocate dummy tail memory for all receive contexts */
dd->rcvhdrtail_dummy_kvaddr = dma_alloc_coherent(&dd->pcidev->dev,
sizeof(u64),
&dd->rcvhdrtail_dummy_dma,
GFP_KERNEL);
if (!dd->rcvhdrtail_dummy_kvaddr) {
dd_dev_err(dd, "cannot allocate dummy tail memory\n");
ret = -ENOMEM;
goto done;
}
The reinit triggered path will overwrite the old allocation and leak it.
Fix by moving the allocation to hfi1_alloc_devdata() and the deallocation
to hfi1_free_devdata().
Link: https://lore.kernel.org/r/20211129192008.101968.91302.stgit@awfm-01.cornelisnetworks.com
Cc: stable@vger.kernel.org
Fixes: 46b010d3ee ("staging/rdma/hfi1: Workaround to prevent corruption during packet delivery")
Signed-off-by: Mike Marciniszyn <mike.marciniszyn@cornelisnetworks.com>
Signed-off-by: Dennis Dalessandro <dennis.dalessandro@cornelisnetworks.com>
Signed-off-by: Jason Gunthorpe <jgg@nvidia.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit b7e945e228 upstream.
The sixth byte of packet data has to be looked up in the sixth group,
not in the seventh one, even if we load the bucket data into ymm6
(and not ymm5, for convenience of tracking stalls).
Without this fix, matching on a MAC address as first field of a set,
if 8-bit groups are selected (due to a small set size) would fail,
that is, the given MAC address would never match.
Reported-by: Nikita Yushchenko <nikita.yushchenko@virtuozzo.com>
Cc: <stable@vger.kernel.org> # 5.6.x
Fixes: 7400b06396 ("nft_set_pipapo: Introduce AVX2-based lookup implementation")
Signed-off-by: Stefano Brivio <sbrivio@redhat.com>
Tested-By: Nikita Yushchenko <nikita.yushchenko@virtuozzo.com>
Signed-off-by: Pablo Neira Ayuso <pablo@netfilter.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 5f719948b5 upstream.
Commit 5fa6863ba6 ("spi: Check we have a spi_device_id for each DT
compatible") added a test to check that every SPI driver has a
spi_device_id for each DT compatiable string defined by the driver
and warns if the spi_device_id is missing. The spi_device_id is
missing for the MMC SPI driver and the following warning is now seen.
WARNING KERN SPI driver mmc_spi has no spi_device_id for mmc-spi-slot
Fix this by adding the necessary spi_device_id.
Signed-off-by: Jon Hunter <jonathanh@nvidia.com>
Link: https://lore.kernel.org/r/20211115113813.238044-1-jonathanh@nvidia.com
Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 27a030e872 upstream.
Commit 5fa6863ba6 ("spi: Check we have a spi_device_id for each DT
compatible") added a test to check that every SPI driver has a
spi_device_id for each DT compatiable string defined by the driver
and warns if the spi_device_id is missing. The spi_device_ids are
missing for the dataflash driver and the following warnings are now
seen.
WARNING KERN SPI driver mtd_dataflash has no spi_device_id for atmel,at45
WARNING KERN SPI driver mtd_dataflash has no spi_device_id for atmel,dataflash
Fix this by adding the necessary spi_device_ids.
Fixes: 96c8395e21 ("spi: Revert modalias changes")
Signed-off-by: Jon Hunter <jonathanh@nvidia.com>
Signed-off-by: Miquel Raynal <miquel.raynal@bootlin.com>
Link: https://lore.kernel.org/linux-mtd/20211130112443.107730-1-jonathanh@nvidia.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 9003fbe0f3 upstream.
Add a HID_QUIRK_NO_INIT_REPORTS quirk for the
Microsoft Surface 3 (non pro) type-cover.
Trying to init the reports seems to confuse the type-cover and
causes 2 issues:
1. Despite hid-multitouch sending the command to switch the
touchpad to multitouch mode, it keeps sending events on the
mouse emulation interface.
2. The touchpad completely stops sending events after a reboot.
Adding the HID_QUIRK_NO_INIT_REPORTS quirk fixes both issues.
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Jiri Kosina <jkosina@suse.cz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 72ee48ee89 upstream.
Currently, the UVC function is activated when open on the corresponding
v4l2 device is called. On another open the activation of the function
fails since the deactivation counter in `usb_function_activate` equals
0. However the error is not returned to userspace since the open of the
v4l2 device is successful.
On a close the function is deactivated (since deactivation counter still
equals 0) and the video is disabled in `uvc_v4l2_release`, although the
UVC application potentially is streaming.
Move activation of UVC function to subscription on UVC_EVENT_SETUP
because there we can guarantee for a userspace application utilizing
UVC. Block subscription on UVC_EVENT_SETUP while another application
already is subscribed to it, indicated by `bool func_connected` in
`struct uvc_device`. Extend the `struct uvc_file_handle` with member
`bool is_uvc_app_handle` to tag it as the handle used by the userspace
UVC application.
With this a process is able to check capabilities of the v4l2 device
without deactivating the function for the actual UVC application.
Reviewed-By: Michael Tretter <m.tretter@pengutronix.de>
Reviewed-by: Laurent Pinchart <laurent.pinchart@ideasonboard.com>
Signed-off-by: Thomas Haemmerle <thomas.haemmerle@wolfvision.net>
Signed-off-by: Michael Tretter <m.tretter@pengutronix.de>
Signed-off-by: Michael Grzeschik <m.grzeschik@pengutronix.de>
Acked-by: Felipe Balbi <balbi@kernel.org>
Link: https://lore.kernel.org/r/20211003201355.24081-1-m.grzeschik@pengutronix.de
Cc: Dan Vacura <W36195@motorola.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit f85e04503f upstream.
Commit f45709df77 ("serial: 8250: Don't touch RTS modem control while
in rs485 mode") sought to prevent user space from interfering with rs485
communication by ignoring a TIOCMSET ioctl() which changes RTS polarity.
It did so in serial8250_do_set_mctrl(), which turns out to be too deep
in the call stack: When a uart_port is opened, RTS polarity is set by
the rs485-aware function uart_port_dtr_rts(). It calls down to
serial8250_do_set_mctrl() and that particular RTS polarity change should
*not* be ignored.
The user-visible result is that on 8250_omap ports which use rs485 with
inverse polarity (RTS bit in MCR register is 1 to receive, 0 to send),
a newly opened port initially sets up RTS for sending instead of
receiving. That's because omap_8250_startup() sets the cached value
up->mcr to 0 and omap_8250_restore_regs() subsequently writes it to the
MCR register. Due to the commit, serial8250_do_set_mctrl() preserves
that incorrect register value:
do_sys_openat2
do_filp_open
path_openat
vfs_open
do_dentry_open
chrdev_open
tty_open
uart_open
tty_port_open
uart_port_activate
uart_startup
uart_port_startup
serial8250_startup
omap_8250_startup # up->mcr = 0
uart_change_speed
serial8250_set_termios
omap_8250_set_termios
omap_8250_restore_regs
serial8250_out_MCR # up->mcr written
tty_port_block_til_ready
uart_dtr_rts
uart_port_dtr_rts
serial8250_set_mctrl
omap8250_set_mctrl
serial8250_do_set_mctrl # mcr[1] = 1 ignored
Fix by intercepting RTS changes from user space in uart_tiocmset()
instead.
Link: https://lore.kernel.org/linux-serial/20211027111644.1996921-1-baocheng.su@siemens.com/
Fixes: f45709df77 ("serial: 8250: Don't touch RTS modem control while in rs485 mode")
Cc: Chao Zeng <chao.zeng@siemens.com>
Cc: stable@vger.kernel.org # v5.7+
Reported-by: Su Bao Cheng <baocheng.su@siemens.com>
Reported-by: Jan Kiszka <jan.kiszka@siemens.com>
Tested-by: Su Bao Cheng <baocheng.su@siemens.com>
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Link: https://lore.kernel.org/r/21170e622a1aaf842a50b32146008b5374b3dd1d.1637596432.git.lukas@wunner.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 00de977f9e upstream.
Commit 761ed4a945 ("tty: serial_core: convert uart_close to use
tty_port_close") converted serial core to use tty_port_close() but
failed to notice that the transmit buffer still needs to be freed on
final close.
Not freeing the transmit buffer means that the buffer is no longer
cleared on next open so that any ioctl() waiting for the buffer to drain
might wait indefinitely (e.g. on termios changes) or that stale data can
end up being transmitted in case tx is restarted.
Furthermore, the buffer of any port that has been opened would leak on
driver unbind.
Note that the port lock is held when clearing the buffer pointer due to
the ldisc race worked around by commit a5ba1d95e4 ("uart: fix race
between uart_put_char() and uart_shutdown()").
Also note that the tty-port shutdown() callback is not called for
console ports so it is not strictly necessary to free the buffer page
after releasing the lock (cf. d72402145a ("tty/serial: do not free
trasnmit buffer page under port lock")).
Link: https://lore.kernel.org/r/319321886d97c456203d5c6a576a5480d07c3478.1635781688.git.baruch@tkos.co.il
Fixes: 761ed4a945 ("tty: serial_core: convert uart_close to use tty_port_close")
Cc: stable@vger.kernel.org # 4.9
Cc: Rob Herring <robh@kernel.org>
Reported-by: Baruch Siach <baruch@tkos.co.il>
Tested-by: Baruch Siach <baruch@tkos.co.il>
Signed-off-by: Johan Hovold <johan@kernel.org>
Link: https://lore.kernel.org/r/20211108085431.12637-1-johan@kernel.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit b40de7469e upstream.
The current implementation uses 0 as lower limit for the baud rate
tolerance for tegra20 and tegra30 chips which causes isses on UART
initialization as soon as baud rate clock is lower than required even
when within the standard UART tolerance of +/- 4%.
This fix aligns the implementation with the initial commit description
of +/- 4% tolerance for tegra chips other than tegra186 and
tegra194.
Fixes: d781ec21ba ("serial: tegra: report clk rate errors")
Cc: stable <stable@vger.kernel.org>
Signed-off-by: Patrik John <patrik.john@u-blox.com>
Link: https://lore.kernel.org/r/sig.19614244f8.20211123132737.88341-1-patrik.john@u-blox.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit ac442a077a upstream.
The document 'ACPI for Arm Components 1.0' defines the following
_HID mappings:
-'Prime cell UART (PL011)': ARMH0011
-'SBSA UART': ARMHB000
Use the sbsa-uart driver when a device is described with
the 'ARMHB000' _HID.
Note:
PL011 devices currently use the sbsa-uart driver instead of the
uart-pl011 driver. Indeed, PL011 devices are not bound to a clock
in ACPI. It is not possible to change their baudrate.
Cc: <stable@vger.kernel.org>
Signed-off-by: Pierre Gondois <Pierre.Gondois@arm.com>
Link: https://lore.kernel.org/r/20211109172248.19061-1-Pierre.Gondois@arm.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 7492ffc90f upstream.
The CONSOLE_POLLING mode is used for tools like k(g)db. In this kind of
setup, it is often sharing a serial device with the normal system console.
This is usually no problem because the polling helpers can consume input
values directly (when in kgdb context) and the normal Linux handlers can
only consume new input values after kgdb switched back.
This is not true anymore when RX DMA is enabled for UARTDM controllers.
Single input values can no longer be received correctly. Instead following
seems to happen:
* on 1. input, some old input is read (continuously)
* on 2. input, two old inputs are read (continuously)
* on 3. input, three old input values are read (continuously)
* on 4. input, 4 previous inputs are received
This repeats then for each group of 4 input values.
This behavior changes slightly depending on what state the controller was
when the first input was received. But this makes working with kgdb
basically impossible because control messages are always corrupted when
kgdboc tries to parse them.
RX DMA should therefore be off when CONSOLE_POLLING is enabled to avoid
these kind of problems. No such problem was noticed for TX DMA.
Fixes: 9969394501 ("tty: serial: msm: Add RX DMA support")
Cc: stable@vger.kernel.org
Signed-off-by: Sven Eckelmann <sven@narfation.org>
Link: https://lore.kernel.org/r/20211113121050.7266-1-sven@narfation.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 51523ed1c2 upstream.
The trampoline_pgd only maps the 0xfffffff000000000-0xffffffffffffffff
range of kernel memory (with 4-level paging). This range contains the
kernel's text+data+bss mappings and the module mapping space but not the
direct mapping and the vmalloc area.
This is enough to get the application processors out of real-mode, but
for code that switches back to real-mode the trampoline_pgd is missing
important parts of the address space. For example, consider this code
from arch/x86/kernel/reboot.c, function machine_real_restart() for a
64-bit kernel:
#ifdef CONFIG_X86_32
load_cr3(initial_page_table);
#else
write_cr3(real_mode_header->trampoline_pgd);
/* Exiting long mode will fail if CR4.PCIDE is set. */
if (boot_cpu_has(X86_FEATURE_PCID))
cr4_clear_bits(X86_CR4_PCIDE);
#endif
/* Jump to the identity-mapped low memory code */
#ifdef CONFIG_X86_32
asm volatile("jmpl *%0" : :
"rm" (real_mode_header->machine_real_restart_asm),
"a" (type));
#else
asm volatile("ljmpl *%0" : :
"m" (real_mode_header->machine_real_restart_asm),
"D" (type));
#endif
The code switches to the trampoline_pgd, which unmaps the direct mapping
and also the kernel stack. The call to cr4_clear_bits() will find no
stack and crash the machine. The real_mode_header pointer below points
into the direct mapping, and dereferencing it also causes a crash.
The reason this does not crash always is only that kernel mappings are
global and the CR3 switch does not flush those mappings. But if theses
mappings are not in the TLB already, the above code will crash before it
can jump to the real-mode stub.
Extend the trampoline_pgd to contain all kernel mappings to prevent
these crashes and to make code which runs on this page-table more
robust.
Signed-off-by: Joerg Roedel <jroedel@suse.de>
Signed-off-by: Borislav Petkov <bp@suse.de>
Cc: stable@vger.kernel.org
Link: https://lkml.kernel.org/r/20211202153226.22946-5-joro@8bytes.org
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit b50db7095f upstream.
There are cases that the TSC clocksource is wrongly judged as unstable by
the clocksource watchdog mechanism which tries to validate the TSC against
HPET, PM_TIMER or jiffies. While there is hardly a general reliable way to
check the validity of a watchdog, Thomas Gleixner proposed [1]:
"I'm inclined to lift that requirement when the CPU has:
1) X86_FEATURE_CONSTANT_TSC
2) X86_FEATURE_NONSTOP_TSC
3) X86_FEATURE_NONSTOP_TSC_S3
4) X86_FEATURE_TSC_ADJUST
5) At max. 4 sockets
After two decades of horrors we're finally at a point where TSC seems
to be halfway reliable and less abused by BIOS tinkerers. TSC_ADJUST
was really key as we can now detect even small modifications reliably
and the important point is that we can cure them as well (not pretty
but better than all other options)."
As feature #3 X86_FEATURE_NONSTOP_TSC_S3 only exists on several generations
of Atom processorz, and is always coupled with X86_FEATURE_CONSTANT_TSC
and X86_FEATURE_NONSTOP_TSC, skip checking it, and also be more defensive
to use maximal 2 sockets.
The check is done inside tsc_init() before registering 'tsc-early' and
'tsc' clocksources, as there were cases that both of them had been
wrongly judged as unreliable.
For more background of tsc/watchdog, there is a good summary in [2]
[tglx} Update vs. jiffies:
On systems where the only remaining clocksource aside of TSC is jiffies
there is no way to make this work because that creates a circular
dependency. Jiffies accuracy depends on not missing a periodic timer
interrupt, which is not guaranteed. That could be detected by TSC, but as
TSC is not trusted this cannot be compensated. The consequence is a
circulus vitiosus which results in shutting down TSC and falling back to
the jiffies clocksource which is even more unreliable.
[1]. https://lore.kernel.org/lkml/87eekfk8bd.fsf@nanos.tec.linutronix.de/
[2]. https://lore.kernel.org/lkml/87a6pimt1f.ffs@nanos.tec.linutronix.de/
[ tglx: Refine comment and amend changelog ]
Fixes: 6e3cd95234 ("x86/hpet: Use another crystalball to evaluate HPET usability")
Suggested-by: Thomas Gleixner <tglx@linutronix.de>
Signed-off-by: Feng Tang <feng.tang@intel.com>
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Cc: "Paul E. McKenney" <paulmck@kernel.org>
Cc: stable@vger.kernel.org
Link: https://lore.kernel.org/r/20211117023751.24190-2-feng.tang@intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 37307f7020 upstream.
In cdnsp_endpoint_init(), cdnsp_ring_alloc() is assigned to pep->ring
and there is a dereference of it in cdnsp_endpoint_init(), which could
lead to a NULL pointer dereference on failure of cdnsp_ring_alloc().
Fix this bug by adding a check of pep->ring.
This bug was found by a static analyzer. The analysis employs
differential checking to identify inconsistent security operations
(e.g., checks or kfrees) between two code paths and confirms that the
inconsistent operations are not recovered in the current function or
the callers, so they constitute bugs.
Note that, as a bug found by static analysis, it can be a false
positive or hard to trigger. Multiple researchers have cross-reviewed
the bug.
Builds with CONFIG_USB_CDNSP_GADGET=y show no new warnings,
and our static analyzer no longer warns about this code.
Fixes: 3d82904559 ("usb: cdnsp: cdns3 Add main part of Cadence USBSSP DRD Driver")
Cc: stable <stable@vger.kernel.org>
Acked-by: Pawel Laszczak <pawell@cadence.com>
Acked-by: Peter Chen <peter.chen@kernel.org>
Signed-off-by: Zhou Qingyang <zhou1615@umn.edu>
Link: https://lore.kernel.org/r/20211130172700.206650-1-zhou1615@umn.edu
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 09f736aa95 upstream.
Turns out some xHC controllers require all 64 bits in the CRCR register
to be written to execute a command abort.
The lower 32 bits containing the command abort bit is written first.
In case the command ring stops before we write the upper 32 bits then
hardware may use these upper bits to set the commnd ring dequeue pointer.
Solve this by making sure the upper 32 bits contain a valid command
ring dequeue pointer.
The original patch that only wrote the first 32 to stop the ring went
to stable, so this fix should go there as well.
Fixes: ff0e50d356 ("xhci: Fix command ring pointer corruption while aborting a command")
Cc: stable@vger.kernel.org
Tested-by: Pavankumar Kondeti <quic_pkondeti@quicinc.com>
Signed-off-by: Mathias Nyman <mathias.nyman@linux.intel.com>
Link: https://lore.kernel.org/r/20211126122340.1193239-2-mathias.nyman@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>